37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 582298 |
Time | |
Date | 200305 |
Day | Fri |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : gso.airport |
State Reference | NC |
Altitude | msl bound lower : 1850 msl bound upper : 2200 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : gso.tracon |
Operator | general aviation : corporate |
Make Model Name | Beechjet 400 |
Operating Under FAR Part | Part 91 |
Navigation In Use | ils localizer & glide slope : 23 other |
Flight Phase | descent : approach |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : corporate |
Function | flight crew : captain oversight : pic |
Qualification | pilot : cfi pilot : atp pilot : multi engine |
Experience | flight time last 90 days : 140 flight time total : 25000 flight time type : 1100 |
ASRS Report | 582298 |
Person 2 | |
Affiliation | company : corporate |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : critical altitude deviation : excursion from assigned altitude non adherence : clearance other anomaly |
Independent Detector | other flight crewa |
Resolutory Action | controller : issued advisory flight crew : regained aircraft control flight crew : overcame equipment problem flight crew : overrode automation |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation |
Narrative:
Autoplt began uncommanded abrupt pitch down. Lost 350 ft before manual recovery. Callback information from reporter revealed the following information: reporter stated that autoplt was in the altitude hold mode, properly annunciated, and the incident happened prior to GS capture. Gso approach alerted them of the deviation about the same time they took action to take manual control. Maintenance inspected and tested the system and was unable to duplicate. Aircraft is back in service.
Original NASA ASRS Text
Title: BE40 AUTOPLT MALFUNCTIONED ON ILS APCH TO GSO. ACFT LOST 350 FT BEFORE RECOVERY.
Narrative: AUTOPLT BEGAN UNCOMMANDED ABRUPT PITCH DOWN. LOST 350 FT BEFORE MANUAL RECOVERY. CALLBACK INFO FROM RPTR REVEALED THE FOLLOWING INFO: RPTR STATED THAT AUTOPLT WAS IN THE ALT HOLD MODE, PROPERLY ANNUNCIATED, AND THE INCIDENT HAPPENED PRIOR TO GS CAPTURE. GSO APCH ALERTED THEM OF THE DEV ABOUT THE SAME TIME THEY TOOK ACTION TO TAKE MANUAL CTL. MAINT INSPECTED AND TESTED THE SYS AND WAS UNABLE TO DUPLICATE. ACFT IS BACK IN SVC.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.