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|
Attributes | |
ACN | 582632 |
Time | |
Date | 200305 |
Day | Mon |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : zzz.airport |
State Reference | US |
Altitude | agl single value : 2500 |
Environment | |
Flight Conditions | VMC |
Light | Dusk |
Aircraft 1 | |
Operator | general aviation : personal |
Make Model Name | Cessna 152 |
Operating Under FAR Part | Part 91 |
Flight Phase | cruise : level |
Flight Plan | None |
Person 1 | |
Affiliation | other |
Function | flight crew : single pilot oversight : pic |
Qualification | pilot : cfi pilot : commercial pilot : instrument pilot : multi engine |
Experience | flight time last 90 days : 100 flight time total : 1200 flight time type : 200 |
ASRS Report | 582632 |
Events | |
Anomaly | aircraft equipment problem : critical maintenance problem : improper documentation maintenance problem : improper maintenance non adherence : published procedure non adherence : far |
Independent Detector | aircraft equipment other aircraft equipment : rpm indicator other other : person 1 |
Resolutory Action | flight crew : landed in emergency condition other |
Consequence | other |
Factors | |
Maintenance | contributing factor : schedule pressure performance deficiency : installation performance deficiency : scheduled maintenance performance deficiency : non compliance with legal requirements performance deficiency : inspection |
Supplementary | |
Problem Areas | Aircraft Maintenance Human Performance |
Primary Problem | Maintenance Human Performance |
Narrative:
I prepared the cessna 152 for a test flight and break-in procedure for the new O-235 power plant. The preflight, starting, and run-up went smoothly. The takeoff was normal in all respects. I backed off the throttle to 75% for the break in procedure. After a shallow cruise climb, I leveled off at 2500 ft AGL and kept the engine at 75% power. After 15 mins of cruise flight and normal operating temperatures, the engine gradually lost most of its power in the span of about 30 seconds. Using the emergency procedures for restart and rough running engine did not solve the problem. I circled to land on a ranch which was below me at the time of the incident. I touched down with full flaps and slowest speed possible. After touchdown, the plane came to a stop in about 300 ft, without any damage. The problem turned out to be the locknut on the rocker arm for the #3 cylinder. The repair was done the next morning by the ia and with permission from the ranch owner, the aircraft was flown back to ZZZ without incident.
Original NASA ASRS Text
Title: A CESSNA 152 AT 2500 FT EXPERIENCED A LOSS OF ENG PWR. MADE AN OFF FIELD LNDG. CAUSED BY #3 CYLINDER ROCKER ARM LOCKNUT FAILURE.
Narrative: I PREPARED THE CESSNA 152 FOR A TEST FLT AND BREAK-IN PROC FOR THE NEW O-235 PWR PLANT. THE PREFLT, STARTING, AND RUN-UP WENT SMOOTHLY. THE TKOF WAS NORMAL IN ALL RESPECTS. I BACKED OFF THE THROTTLE TO 75% FOR THE BREAK IN PROC. AFTER A SHALLOW CRUISE CLB, I LEVELED OFF AT 2500 FT AGL AND KEPT THE ENG AT 75% PWR. AFTER 15 MINS OF CRUISE FLT AND NORMAL OPERATING TEMPS, THE ENG GRADUALLY LOST MOST OF ITS PWR IN THE SPAN OF ABOUT 30 SECONDS. USING THE EMER PROCS FOR RESTART AND ROUGH RUNNING ENG DID NOT SOLVE THE PROB. I CIRCLED TO LAND ON A RANCH WHICH WAS BELOW ME AT THE TIME OF THE INCIDENT. I TOUCHED DOWN WITH FULL FLAPS AND SLOWEST SPD POSSIBLE. AFTER TOUCHDOWN, THE PLANE CAME TO A STOP IN ABOUT 300 FT, WITHOUT ANY DAMAGE. THE PROB TURNED OUT TO BE THE LOCKNUT ON THE ROCKER ARM FOR THE #3 CYLINDER. THE REPAIR WAS DONE THE NEXT MORNING BY THE IA AND WITH PERMISSION FROM THE RANCH OWNER, THE ACFT WAS FLOWN BACK TO ZZZ WITHOUT INCIDENT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.