Narrative:

After takeoff from seatac the left main gear failed to retract normally. The right main and nose gear did retract normally. Through proper use of the checklist it was discovered that the floor mounted alternate gear extension door was somehow left partially open and then covered by the cockpit garbage bag. Upon closing the door, the gear operated normally and the flight was successfully completed.

Google
 

Original NASA ASRS Text

Title: WHEN UNABLE TO RETRACT THE L MAIN GEAR, THE FLT CREW OF DH8 DISCOVERED THE ALTERNATE GEAR EXTENSION DOOR IN THE COCKPIT FLOOR WAS OPEN THUS DEACTIVATING THE PRIMARY SYS. UPON CLOSING THE DOOR, PER THE ABNORMAL CHKLIST, THE RETRACT MECHANISM RETURNED TO NORMAL.

Narrative: AFTER TKOF FROM SEATAC THE L MAIN GEAR FAILED TO RETRACT NORMALLY. THE R MAIN AND NOSE GEAR DID RETRACT NORMALLY. THROUGH PROPER USE OF THE CHKLIST IT WAS DISCOVERED THAT THE FLOOR MOUNTED ALTERNATE GEAR EXTENSION DOOR WAS SOMEHOW LEFT PARTIALLY OPEN AND THEN COVERED BY THE COCKPIT GARBAGE BAG. UPON CLOSING THE DOOR, THE GEAR OPERATED NORMALLY AND THE FLT WAS SUCCESSFULLY COMPLETED.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.