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|
Attributes | |
ACN | 597259 |
Time | |
Date | 200310 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : zzz.airport |
State Reference | US |
Altitude | agl single value : 0 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Operator | general aviation : personal |
Make Model Name | Bonanza 35 |
Operating Under FAR Part | Part 91 |
Flight Phase | ground : maintenance ground : parked |
Flight Plan | VFR |
Person 1 | |
Affiliation | other |
Function | flight crew : single pilot |
Qualification | pilot : private |
Experience | flight time last 90 days : 50 flight time total : 600 flight time type : 50 |
ASRS Report | 597259 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other other : person 1 |
Resolutory Action | none taken : detected after the fact |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft Airport Flight Crew Human Performance Environmental Factor |
Primary Problem | Airport |
Narrative:
Oct/thu/03, I departed ZZZ at XA30 local time and arrived ZZZ1 at XC30 local time. Tied the aircraft down, a 1964 BE35. Returned oct/sun/03, at XA30 local time, and found 2 wires had been cut on the alternator, one spark plug wire, and an upper trim tab control cable on the left ruddervator had been cut 1/2 way through, along with a knife hole in the bottom of the left ruddervator. We fixed the spark plug wire using a solderless crimp type connector, reattached the outer ground sheath and taped it up. Used the same type connectors to fix the 2 small cut wires on the alternator. I made the repairs to bring the airplane home as there were no services at the airport, not even a payphone! I deemed the aircraft safe to bring home for repair and after an expensive preflight and long run-up period. I took off and gained extra altitude on climb out -- watching and listening to everything! The return flight was uneventful. I realize I should not have made the repairs to the airplane, but there were no services and I am a builder/owner/pilot of an rv-6A and a mechanic for a living. I felt confident in my decision to bring it home for proper work.
Original NASA ASRS Text
Title: A BEECH-35 WHILE PARKED OVERNIGHT INCURRED DAMAGE TO WIRING ON THE ALTERNATOR AND ONE SPARK PLUG WIRE. TRIM TAB CTL CABLE HAD BEEN CUT HALFWAY AND A KNIFE HOLE IN THE L RUDDERVATOR.
Narrative: OCT/THU/03, I DEPARTED ZZZ AT XA30 LCL TIME AND ARRIVED ZZZ1 AT XC30 LCL TIME. TIED THE ACFT DOWN, A 1964 BE35. RETURNED OCT/SUN/03, AT XA30 LCL TIME, AND FOUND 2 WIRES HAD BEEN CUT ON THE ALTERNATOR, ONE SPARK PLUG WIRE, AND AN UPPER TRIM TAB CTL CABLE ON THE L RUDDERVATOR HAD BEEN CUT 1/2 WAY THROUGH, ALONG WITH A KNIFE HOLE IN THE BOTTOM OF THE L RUDDERVATOR. WE FIXED THE SPARK PLUG WIRE USING A SOLDERLESS CRIMP TYPE CONNECTOR, REATTACHED THE OUTER GND SHEATH AND TAPED IT UP. USED THE SAME TYPE CONNECTORS TO FIX THE 2 SMALL CUT WIRES ON THE ALTERNATOR. I MADE THE REPAIRS TO BRING THE AIRPLANE HOME AS THERE WERE NO SVCS AT THE ARPT, NOT EVEN A PAYPHONE! I DEEMED THE ACFT SAFE TO BRING HOME FOR REPAIR AND AFTER AN EXPENSIVE PREFLT AND LONG RUN-UP PERIOD. I TOOK OFF AND GAINED EXTRA ALT ON CLBOUT -- WATCHING AND LISTENING TO EVERYTHING! THE RETURN FLT WAS UNEVENTFUL. I REALIZE I SHOULD NOT HAVE MADE THE REPAIRS TO THE AIRPLANE, BUT THERE WERE NO SVCS AND I AM A BUILDER/OWNER/PLT OF AN RV-6A AND A MECH FOR A LIVING. I FELT CONFIDENT IN MY DECISION TO BRING IT HOME FOR PROPER WORK.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.