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|
Attributes | |
ACN | 621802 |
Time | |
Date | 200406 |
Day | Fri |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : pdx.airport |
State Reference | OR |
Altitude | msl single value : 6000 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : p80.tracon tower : mggt.tower |
Operator | common carrier : air carrier |
Make Model Name | B737-500 |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : intermediate altitude |
Route In Use | departure sid : n/s |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : multi engine pilot : instrument |
Experience | flight time last 90 days : 200 flight time total : 8500 flight time type : 5500 |
ASRS Report | 621802 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Events | |
Anomaly | aircraft equipment problem : critical non adherence other other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : door warning sys other flight crewa |
Resolutory Action | flight crew : landed as precaution other |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
On takeoff from pdx, we noticed immediately that the aircraft was not pressurizing. We checked to see that the appropriate switches were in the correct position, and found that the pressurization control panel was properly configured, and that the outflow valve was fully closed. We elected to level off at 8000 ft to further investigate the problem. Passing about 5000 ft, we got an autofail light for the pressurization system, and switched to standby. Passing 6000 ft, the equipment door light came on, which convinced us the door had somehow come open in-flight, preventing the aircraft from pressurizing. The captain tried to talk to dispatch, but cold not get a good phone patch, we suspect due to our altitude. We informed pdx operations of our situation and elected to return to pdx for what would be an overweight landing (approximately 116000 pounds). The landing was uneventful, and we returned to the chocks at pdx where maintenance assisted us with checking the equipment bay door and checking for hot brakes. Once everything was checked out and we received more fuel, we continued with our flight to den uneventfully.
Original NASA ASRS Text
Title: B737-500 RETURNS TO PDX FOR OVERWT LNDG WHEN UNABLE TO PRESSURIZE DUE TO IMPROPERLY SECURED EQUIP ACCESS DOOR.
Narrative: ON TKOF FROM PDX, WE NOTICED IMMEDIATELY THAT THE ACFT WAS NOT PRESSURIZING. WE CHKED TO SEE THAT THE APPROPRIATE SWITCHES WERE IN THE CORRECT POS, AND FOUND THAT THE PRESSURIZATION CTL PANEL WAS PROPERLY CONFIGURED, AND THAT THE OUTFLOW VALVE WAS FULLY CLOSED. WE ELECTED TO LEVEL OFF AT 8000 FT TO FURTHER INVESTIGATE THE PROB. PASSING ABOUT 5000 FT, WE GOT AN AUTOFAIL LIGHT FOR THE PRESSURIZATION SYS, AND SWITCHED TO STANDBY. PASSING 6000 FT, THE EQUIP DOOR LIGHT CAME ON, WHICH CONVINCED US THE DOOR HAD SOMEHOW COME OPEN INFLT, PREVENTING THE ACFT FROM PRESSURIZING. THE CAPT TRIED TO TALK TO DISPATCH, BUT COLD NOT GET A GOOD PHONE PATCH, WE SUSPECT DUE TO OUR ALT. WE INFORMED PDX OPS OF OUR SIT AND ELECTED TO RETURN TO PDX FOR WHAT WOULD BE AN OVERWT LNDG (APPROX 116000 LBS). THE LNDG WAS UNEVENTFUL, AND WE RETURNED TO THE CHOCKS AT PDX WHERE MAINT ASSISTED US WITH CHKING THE EQUIP BAY DOOR AND CHKING FOR HOT BRAKES. ONCE EVERYTHING WAS CHKED OUT AND WE RECEIVED MORE FUEL, WE CONTINUED WITH OUR FLT TO DEN UNEVENTFULLY.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.