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|
Attributes | |
ACN | 622303 |
Time | |
Date | 200307 |
Day | Tue |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : okc.airport |
State Reference | OK |
Altitude | agl single value : 100 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : okc.tower |
Operator | common carrier : air carrier |
Make Model Name | B737 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : takeoff climbout : initial descent : approach descent other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 220 flight time total : 20000 flight time type : 1000 |
ASRS Report | 622303 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : multi engine pilot : instrument |
Experience | flight time last 90 days : 250 flight time total : 7000 flight time type : 1700 |
ASRS Report | 622306 |
Events | |
Anomaly | aircraft equipment problem : less severe |
Independent Detector | aircraft equipment other aircraft equipment : lndg gear indication , lndg gear handle other flight crewa other flight crewb |
Resolutory Action | flight crew : diverted to another airport flight crew : landed as precaution other |
Consequence | other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
After takeoff, landing gear would not come up. Landing gear lever would not go above 'off' position. Landing gear override trigger was pulled, gear still did not come up. Aircraft returned to okc. Checklist was run for the problem. Aircraft landed at okc, overweight landing at 116200 pounds. Supplemental information from acn 622306: aircraft was leveled off in VMC at 5000 ft MSL. Qrc checklist was run with no results. 'Trigger pull' was accomplished in accordance with the checklist. Both pilots attempted to 'trigger pull,' gear handle still would not go beyond 'off' position. Landed the aircraft uneventfully at okc approximately 2000 pounds overweight (116200 pounds).
Original NASA ASRS Text
Title: B737 CREW WAS UNABLE TO RETRACT THE LNDG GEAR AFTER TKOF AT OKC.
Narrative: AFTER TKOF, LNDG GEAR WOULD NOT COME UP. LNDG GEAR LEVER WOULD NOT GO ABOVE 'OFF' POS. LNDG GEAR OVERRIDE TRIGGER WAS PULLED, GEAR STILL DID NOT COME UP. ACFT RETURNED TO OKC. CHKLIST WAS RUN FOR THE PROB. ACFT LANDED AT OKC, OVERWT LNDG AT 116200 LBS. SUPPLEMENTAL INFO FROM ACN 622306: ACFT WAS LEVELED OFF IN VMC AT 5000 FT MSL. QRC CHKLIST WAS RUN WITH NO RESULTS. 'TRIGGER PULL' WAS ACCOMPLISHED IN ACCORDANCE WITH THE CHKLIST. BOTH PLTS ATTEMPTED TO 'TRIGGER PULL,' GEAR HANDLE STILL WOULD NOT GO BEYOND 'OFF' POS. LANDED THE ACFT UNEVENTFULLY AT OKC APPROX 2000 LBS OVERWT (116200 LBS).
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.