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|
Attributes | |
ACN | 628207 |
Time | |
Date | 200408 |
Day | Tue |
Place | |
Locale Reference | airport : zzz.airport |
State Reference | US |
Aircraft 1 | |
Make Model Name | King Air C90 E90 |
Operating Under FAR Part | Part 91 |
Flight Phase | ground : maintenance |
Person 1 | |
Function | maintenance : technician |
Qualification | technician : powerplant technician : inspection authority technician : airframe |
Experience | maintenance lead technician : 5 maintenance technician : 5 |
ASRS Report | 628207 |
Events | |
Anomaly | maintenance problem : improper maintenance maintenance problem : improper documentation non adherence : published procedure non adherence : far other anomaly other |
Independent Detector | other other : 1 |
Resolutory Action | none taken : detected after the fact |
Consequence | other other |
Supplementary | |
Problem Areas | Company Maintenance Human Performance Aircraft |
Primary Problem | Maintenance Human Performance |
Narrative:
While performing an 'inspection after encountering turbulence' on a usda forest service fire fighting aircraft, as the wing upper forward mount bolts and nuts were being torqued, the torque wrench being used broke. Another torque wrench was obtained, but it was noticed that it was out of calibration. Myself and the technician who was performing the work discussed this and 'rationalized' that 'it was only out of calibration by a month of two.' it was decided to continue with the procedure with the out of calibration torque wrench. When brought to my attention yesterday evening I immediately arranged to have the aircraft grounded and a torque check done. I don't want to sound like I'm making excuses, but I believe this occurrence is a result of fatigue and stress. During the previous 7 days, both myself and the other technician had worked many long hours. Over the previous 30 days I have had 3 days off. On my part, a high degree of stress was also felt resulting from the discovery that these bolts had previously been improperly installed approximately 110 hours before by one shop, and that a re-torque check had been accomplished about 70 hours after that by another shop. If the aircraft had not flown through the turbulence, resulting in the need for the turbulence inspection, this aircraft would not have had these bolts checked for another 900 hours, which would have undoubtedly resulted in the loss of one of my pilots and the aircraft. In hindsight, I should have recognized then that I was badly in need of some rest. Instead, I pressed on. While I was not personally performing this work I feel responsible for this mistake, as I was probably instrumental in convincing the technician who was, into using the un-calibrated torque wrench. I have advised him to also submit a report.
Original NASA ASRS Text
Title: A BE90, DURING A TURB ENCOUNTER INSPECTION WAS FOUND TO HAVE THE WING UPPER FORWARD MOUNT BOLTS TORQUE CHKED WITH AN UNCALIBRATED TORQUE WRENCH.
Narrative: WHILE PERFORMING AN 'INSPECTION AFTER ENCOUNTERING TURB' ON A USDA FOREST SVC FIRE FIGHTING ACFT, AS THE WING UPPER FORWARD MOUNT BOLTS AND NUTS WERE BEING TORQUED, THE TORQUE WRENCH BEING USED BROKE. ANOTHER TORQUE WRENCH WAS OBTAINED, BUT IT WAS NOTICED THAT IT WAS OUT OF CALIBRATION. MYSELF AND THE TECHNICIAN WHO WAS PERFORMING THE WORK DISCUSSED THIS AND 'RATIONALIZED' THAT 'IT WAS ONLY OUT OF CALIBRATION BY A MONTH OF TWO.' IT WAS DECIDED TO CONTINUE WITH THE PROC WITH THE OUT OF CALIBRATION TORQUE WRENCH. WHEN BROUGHT TO MY ATTN YESTERDAY EVENING I IMMEDIATELY ARRANGED TO HAVE THE ACFT GNDED AND A TORQUE CHK DONE. I DON'T WANT TO SOUND LIKE I'M MAKING EXCUSES, BUT I BELIEVE THIS OCCURRENCE IS A RESULT OF FATIGUE AND STRESS. DURING THE PREVIOUS 7 DAYS, BOTH MYSELF AND THE OTHER TECHNICIAN HAD WORKED MANY LONG HRS. OVER THE PREVIOUS 30 DAYS I HAVE HAD 3 DAYS OFF. ON MY PART, A HIGH DEGREE OF STRESS WAS ALSO FELT RESULTING FROM THE DISCOVERY THAT THESE BOLTS HAD PREVIOUSLY BEEN IMPROPERLY INSTALLED APPROX 110 HRS BEFORE BY ONE SHOP, AND THAT A RE-TORQUE CHK HAD BEEN ACCOMPLISHED ABOUT 70 HRS AFTER THAT BY ANOTHER SHOP. IF THE ACFT HAD NOT FLOWN THROUGH THE TURB, RESULTING IN THE NEED FOR THE TURB INSPECTION, THIS ACFT WOULD NOT HAVE HAD THESE BOLTS CHKED FOR ANOTHER 900 HRS, WHICH WOULD HAVE UNDOUBTEDLY RESULTED IN THE LOSS OF ONE OF MY PLTS AND THE ACFT. IN HINDSIGHT, I SHOULD HAVE RECOGNIZED THEN THAT I WAS BADLY IN NEED OF SOME REST. INSTEAD, I PRESSED ON. WHILE I WAS NOT PERSONALLY PERFORMING THIS WORK I FEEL RESPONSIBLE FOR THIS MISTAKE, AS I WAS PROBABLY INSTRUMENTAL IN CONVINCING THE TECHNICIAN WHO WAS, INTO USING THE UN-CALIBRATED TORQUE WRENCH. I HAVE ADVISED HIM TO ALSO SUBMIT A RPT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.