Narrative:

After being cleared for pushback by ground and releasing the brakes, the tug driver told us that a maintenance manager had stopped the push. We queried maintenance manager on the radio and they did not know why. We later found out that the aircraft had been borescoped (#2 engine) and that the signoffs for the work had not been completed. Maintenance opened the cowl to ensure that the plug had been safetied, and it had. My problem with this situation was that we were improperly dispatched from a maintenance standpoint, and that if someone in maintenance had not 'caught' this, the plug had not in fact been installed, we could have had a catastrophic engine failure due to a maintenance oversight.

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Original NASA ASRS Text

Title: A B777-200 WAS PUSHED BACK OFF A GATE, BUT HALTED BY MAINT REQUEST. BORESCOPE ACCOMPLISHED, BUT NO SIGNOFF FOR PLUG INSTALLATION AND SAFETY.

Narrative: AFTER BEING CLRED FOR PUSHBACK BY GND AND RELEASING THE BRAKES, THE TUG DRIVER TOLD US THAT A MAINT MGR HAD STOPPED THE PUSH. WE QUERIED MAINT MGR ON THE RADIO AND THEY DID NOT KNOW WHY. WE LATER FOUND OUT THAT THE ACFT HAD BEEN BORESCOPED (#2 ENG) AND THAT THE SIGNOFFS FOR THE WORK HAD NOT BEEN COMPLETED. MAINT OPENED THE COWL TO ENSURE THAT THE PLUG HAD BEEN SAFETIED, AND IT HAD. MY PROB WITH THIS SIT WAS THAT WE WERE IMPROPERLY DISPATCHED FROM A MAINT STANDPOINT, AND THAT IF SOMEONE IN MAINT HAD NOT 'CAUGHT' THIS, THE PLUG HAD NOT IN FACT BEEN INSTALLED, WE COULD HAVE HAD A CATASTROPHIC ENG FAILURE DUE TO A MAINT OVERSIGHT.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.