37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 634101 |
Time | |
Date | 200410 |
Day | Sun |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : zzz.airport |
State Reference | US |
Environment | |
Flight Conditions | VMC |
Weather Elements | Rain |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air taxi |
Make Model Name | Jet Ranger III |
Operating Under FAR Part | Part 135 |
Flight Phase | climbout : takeoff ground : preflight |
Flight Plan | VFR |
Person 1 | |
Affiliation | company : air taxi |
Function | flight crew : single pilot |
Qualification | pilot : instrument pilot : commercial |
Experience | flight time last 90 days : 65 flight time total : 4938 flight time type : 2693 |
ASRS Report | 634101 |
Person 2 | |
Affiliation | company : air taxi |
Events | |
Anomaly | non adherence : published procedure non adherence : company policies |
Independent Detector | other flight crewa |
Resolutory Action | none taken : detected after the fact |
Supplementary | |
Problem Areas | Flight Crew Human Performance |
Primary Problem | Flight Crew Human Performance |
Narrative:
Received a call. Crew and myself went to aircraft. Crew hooked up battery cart, I started aircraft and thought I had given the unhook signal to crew member as he was unhooking heater and lines. Ran up aircraft, turned all radios on. Crew was in the aircraft at this time. Lifted off and started hovering out and nose of aircraft pulled down. I stopped and realized that the cart was still hooked up. Returned to pad and found cart overturned and plug on cart broken. Aircraft was checked. No damage was found. Cause: complacency. Corrective actions: keep a crew member at the cart till start is completed and unhook signal is given then unhook landlines, and heaters.
Original NASA ASRS Text
Title: BH206 HELI PLT DID NOT DISCONNECT THE BATTERY CART BEFORE LIFTOFF.
Narrative: RECEIVED A CALL. CREW AND MYSELF WENT TO ACFT. CREW HOOKED UP BATTERY CART, I STARTED ACFT AND THOUGHT I HAD GIVEN THE UNHOOK SIGNAL TO CREW MEMBER AS HE WAS UNHOOKING HEATER AND LINES. RAN UP ACFT, TURNED ALL RADIOS ON. CREW WAS IN THE ACFT AT THIS TIME. LIFTED OFF AND STARTED HOVERING OUT AND NOSE OF ACFT PULLED DOWN. I STOPPED AND REALIZED THAT THE CART WAS STILL HOOKED UP. RETURNED TO PAD AND FOUND CART OVERTURNED AND PLUG ON CART BROKEN. ACFT WAS CHKED. NO DAMAGE WAS FOUND. CAUSE: COMPLACENCY. CORRECTIVE ACTIONS: KEEP A CREW MEMBER AT THE CART TILL START IS COMPLETED AND UNHOOK SIGNAL IS GIVEN THEN UNHOOK LANDLINES, AND HEATERS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.