37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 640821 |
Time | |
Date | 200412 |
Day | Fri |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : zzz.airport |
State Reference | US |
Altitude | agl single value : 0 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | B737-700 |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : maintenance |
Person 1 | |
Affiliation | company : air carrier |
Function | maintenance : lead technician |
Qualification | technician : airframe technician : powerplant |
ASRS Report | 640821 |
Person 2 | |
Affiliation | company : air carrier |
Function | maintenance : technician |
Events | |
Anomaly | aircraft equipment problem : less severe maintenance problem : non compliance with mel non adherence : far non adherence : published procedure |
Independent Detector | aircraft equipment other aircraft equipment : left duct press. ind. other other : 969 |
Consequence | other other |
Factors | |
Maintenance | contributing factor : schedule pressure performance deficiency : logbook entry performance deficiency : fault isolation performance deficiency : non compliance with legal requirements |
Supplementary | |
Problem Areas | Aircraft Maintenance Human Performance |
Primary Problem | Maintenance Human Performance |
Situations | |
Publication | MINIMUM EQUIP. LIST |
Narrative:
Were advised early that aircraft was arriving with dual bleed trip and that aircraft would be late. #1 engine had history of bleed trips and were advised that we would not work the item. So aircraft proceeded to lock out the bleed valve (prsov). Instead we locked out the high stage valve. We ran the engines to make sure no other bleed trips appeared. At the time #1 engine bleed valve was off. No problems were noted and the plane was moved to another line and a different gate. The contributing factors were bad WX and a shift change going on, so trying to be expedient, we made the mistake of locking out the wrong valve. Also, our fail safe engine run should have caught the mistake and we missed that as well.
Original NASA ASRS Text
Title: A B737-700 WITH HISTORY OF #1 BLEED OVERHEAT TRIPS HAD THE PRESSURE REGULATOR SHUTOFF VALVE DEFERRED AS INOP PER THE MEL. DISPATCHED WITH THE WRONG VALVE LOCKED OUT.
Narrative: WERE ADVISED EARLY THAT ACFT WAS ARRIVING WITH DUAL BLEED TRIP AND THAT ACFT WOULD BE LATE. #1 ENG HAD HISTORY OF BLEED TRIPS AND WERE ADVISED THAT WE WOULD NOT WORK THE ITEM. SO ACFT PROCEEDED TO LOCK OUT THE BLEED VALVE (PRSOV). INSTEAD WE LOCKED OUT THE HIGH STAGE VALVE. WE RAN THE ENGS TO MAKE SURE NO OTHER BLEED TRIPS APPEARED. AT THE TIME #1 ENG BLEED VALVE WAS OFF. NO PROBS WERE NOTED AND THE PLANE WAS MOVED TO ANOTHER LINE AND A DIFFERENT GATE. THE CONTRIBUTING FACTORS WERE BAD WX AND A SHIFT CHANGE GOING ON, SO TRYING TO BE EXPEDIENT, WE MADE THE MISTAKE OF LOCKING OUT THE WRONG VALVE. ALSO, OUR FAIL SAFE ENG RUN SHOULD HAVE CAUGHT THE MISTAKE AND WE MISSED THAT AS WELL.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.