37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 667213 |
Time | |
Date | 200508 |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : rkd.airport |
State Reference | ME |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air taxi |
Make Model Name | Beech 1900 |
Operating Under FAR Part | Part 135 |
Flight Phase | ground : takeoff roll |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air taxi |
Function | flight crew : captain oversight : pic |
Qualification | pilot : multi engine pilot : instrument pilot : cfi pilot : atp |
Experience | flight time last 90 days : 170 flight time total : 3700 flight time type : 2500 |
ASRS Report | 667213 |
Person 2 | |
Affiliation | company : air taxi |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : overcame equipment problem flight crew : overrode automation flight crew : regained aircraft control |
Consequence | other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
We were departing runway 21 at rockland; me; en route to augusta; me; a distance of less than 30 mi. When my first officer called 'V1; rotate' at 100 KIAS; I pulled on the yoke with both hands and it did not move. It was stuck; and I pulled significantly harder. Something in the system released; the yoke moved quickly aft and the aircraft jumped into the air. Rather than return to rkd; which had men and equipment working on runway 13/31 (the longer runway); I elected to continue to augusta; only 12 mins away. All was normal en route except the elevator trim moved very slowly to nose up; requiring about 1/2 unit nose down trim every 1-2 mins. After landing in augusta; a flight control check and an external inspection revealed no abnormalities. I entered the event in the maintenance log immediately and contacted my company. Callback conversation with reporter revealed the following information: reporter advised that due to the primary flight control write-up made at the conclusion of the flight; the FAA investigated and has determined this event to be an official incident. The initial determination of the cause of the problem is some missing fasteners on 1 elevator hinge.
Original NASA ASRS Text
Title: FLT CREW OF BE19 ENCOUNTER STUCK ELEVATOR ON ROTATION. EXTRA FORCE RELEASES THE CTLS AND THE FLT CONTINUES TO A MORE SUITABLE ARPT (THEIR DEST) WHERE THEY LAND AND SEEK MAINT.
Narrative: WE WERE DEPARTING RWY 21 AT ROCKLAND; ME; ENRTE TO AUGUSTA; ME; A DISTANCE OF LESS THAN 30 MI. WHEN MY FO CALLED 'V1; ROTATE' AT 100 KIAS; I PULLED ON THE YOKE WITH BOTH HANDS AND IT DID NOT MOVE. IT WAS STUCK; AND I PULLED SIGNIFICANTLY HARDER. SOMETHING IN THE SYS RELEASED; THE YOKE MOVED QUICKLY AFT AND THE ACFT JUMPED INTO THE AIR. RATHER THAN RETURN TO RKD; WHICH HAD MEN AND EQUIP WORKING ON RWY 13/31 (THE LONGER RWY); I ELECTED TO CONTINUE TO AUGUSTA; ONLY 12 MINS AWAY. ALL WAS NORMAL ENRTE EXCEPT THE ELEVATOR TRIM MOVED VERY SLOWLY TO NOSE UP; REQUIRING ABOUT 1/2 UNIT NOSE DOWN TRIM EVERY 1-2 MINS. AFTER LNDG IN AUGUSTA; A FLT CTL CHK AND AN EXTERNAL INSPECTION REVEALED NO ABNORMALITIES. I ENTERED THE EVENT IN THE MAINT LOG IMMEDIATELY AND CONTACTED MY COMPANY. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: RPTR ADVISED THAT DUE TO THE PRIMARY FLT CTL WRITE-UP MADE AT THE CONCLUSION OF THE FLT; THE FAA INVESTIGATED AND HAS DETERMINED THIS EVENT TO BE AN OFFICIAL INCIDENT. THE INITIAL DETERMINATION OF THE CAUSE OF THE PROB IS SOME MISSING FASTENERS ON 1 ELEVATOR HINGE.
Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.