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|
Attributes | |
ACN | 690595 |
Time | |
Date | 200603 |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : cmh.airport |
State Reference | OH |
Altitude | agl single value : 0 |
Environment | |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tower : sea.tower |
Operator | common carrier : air carrier |
Make Model Name | EMB ERJ 145 ER&LR |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : parked |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 690595 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Events | |
Anomaly | non adherence : company policies non adherence : published procedure |
Independent Detector | other other : 3 |
Resolutory Action | none taken : detected after the fact |
Supplementary | |
Problem Areas | Aircraft Flight Crew Human Performance |
Primary Problem | Flight Crew Human Performance |
Narrative:
After deplaning on a termination flight in cmh; I got off the plane; briefly helped the agent get a few valet bags to the passenger; and was going back onto the plane to finish post-flight when one of the ramp personnel pointed out that an engine was still running. I found that the switch for the #2 was still on; and the rest of the switches were in the correct position. I also remembered that we had not done a parking checklist and so I verified that everything was accomplished. I think a number of factors contributed; but the main one being fatigue. I had been up since early so that I could commute for an XA20 departure; and it was XM30 at the time of this error. I felt fatigued. Also; the ground power was hooked up during the parking flow; and I remember getting it turned on right away to save fuel; but I allowed it to interrupt my normal flow and never came back to that part of the parking flow. Also; at the same time; I was interested in knowing whether maintenance wanted the plane completely shut down or not; and the rest of the crew quickly began packing up and calling the hotel; as it had been a long day for all of us. There is plenty of emphasis on checklist completion. I should have commuted down the day prior knowing that it was going to be a long day even without a commute.
Original NASA ASRS Text
Title: FATIGUED E140 FLT CREW DEPLANES WITHOUT SHUTTING DOWN THE #2 ENG.
Narrative: AFTER DEPLANING ON A TERMINATION FLT IN CMH; I GOT OFF THE PLANE; BRIEFLY HELPED THE AGENT GET A FEW VALET BAGS TO THE PAX; AND WAS GOING BACK ONTO THE PLANE TO FINISH POST-FLT WHEN ONE OF THE RAMP PERSONNEL POINTED OUT THAT AN ENG WAS STILL RUNNING. I FOUND THAT THE SWITCH FOR THE #2 WAS STILL ON; AND THE REST OF THE SWITCHES WERE IN THE CORRECT POS. I ALSO REMEMBERED THAT WE HAD NOT DONE A PARKING CHKLIST AND SO I VERIFIED THAT EVERYTHING WAS ACCOMPLISHED. I THINK A NUMBER OF FACTORS CONTRIBUTED; BUT THE MAIN ONE BEING FATIGUE. I HAD BEEN UP SINCE EARLY SO THAT I COULD COMMUTE FOR AN XA20 DEP; AND IT WAS XM30 AT THE TIME OF THIS ERROR. I FELT FATIGUED. ALSO; THE GND PWR WAS HOOKED UP DURING THE PARKING FLOW; AND I REMEMBER GETTING IT TURNED ON RIGHT AWAY TO SAVE FUEL; BUT I ALLOWED IT TO INTERRUPT MY NORMAL FLOW AND NEVER CAME BACK TO THAT PART OF THE PARKING FLOW. ALSO; AT THE SAME TIME; I WAS INTERESTED IN KNOWING WHETHER MAINT WANTED THE PLANE COMPLETELY SHUT DOWN OR NOT; AND THE REST OF THE CREW QUICKLY BEGAN PACKING UP AND CALLING THE HOTEL; AS IT HAD BEEN A LONG DAY FOR ALL OF US. THERE IS PLENTY OF EMPHASIS ON CHKLIST COMPLETION. I SHOULD HAVE COMMUTED DOWN THE DAY PRIOR KNOWING THAT IT WAS GOING TO BE A LONG DAY EVEN WITHOUT A COMMUTE.
Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.