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|
Attributes | |
ACN | 695114 |
Time | |
Date | 200604 |
Local Time Of Day | 0001 To 0600 |
Place | |
Locale Reference | atc facility : zzz.artcc |
State Reference | US |
Altitude | msl single value : 32000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zzz.artcc |
Operator | common carrier : air carrier |
Make Model Name | DC-10 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | cruise : level |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 150 flight time total : 25000 flight time type : 6000 |
ASRS Report | 695114 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : cfi pilot : flight engineer pilot : atp |
Experience | flight time last 90 days : 50 flight time total : 1300 flight time type : 50 |
ASRS Report | 694879 |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : #3 eng vibration other flight crewa other flight crewb |
Resolutory Action | controller : provided flight assist controller : issued new clearance flight crew : landed as precaution flight crew : diverted to another airport flight crew : declared emergency |
Supplementary | |
Problem Areas | Aircraft Flight Crew Human Performance |
Primary Problem | Aircraft |
Narrative:
2 hours after departure from ZZZ #3 engine annunciated high vibes. Gauge was more than level 3 on both a and B pick-ups. We shut down #3 in accordance with checklist and turned right towards our point of origin. We descended while notifying ATC and were cleared to FL220. We requested return to ZZZ as the safest course of action. An attempt to dump fuel was aborted when #3 tank would not dump. We landed approximately 30000 pounds overweight at 398000 pounds without incident. An emergency was declared on initial notification to ATC while turning back and descending.
Original NASA ASRS Text
Title: DC10 FLT CREW HAS MALFUNCTION OF THE #3 ENG; SECURES ENG; DECLARES AN EMER AND DIVERTS FOR LNDG.
Narrative: 2 HRS AFTER DEP FROM ZZZ #3 ENG ANNUNCIATED HIGH VIBES. GAUGE WAS MORE THAN LEVEL 3 ON BOTH A AND B PICK-UPS. WE SHUT DOWN #3 IN ACCORDANCE WITH CHKLIST AND TURNED R TOWARDS OUR POINT OF ORIGIN. WE DSNDED WHILE NOTIFYING ATC AND WERE CLRED TO FL220. WE REQUESTED RETURN TO ZZZ AS THE SAFEST COURSE OF ACTION. AN ATTEMPT TO DUMP FUEL WAS ABORTED WHEN #3 TANK WOULD NOT DUMP. WE LANDED APPROX 30000 LBS OVERWT AT 398000 LBS WITHOUT INCIDENT. AN EMER WAS DECLARED ON INITIAL NOTIFICATION TO ATC WHILE TURNING BACK AND DSNDING.
Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.