37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 714003 |
Time | |
Date | 200610 |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : zmp.artcc |
State Reference | MN |
Altitude | msl single value : 21000 |
Environment | |
Flight Conditions | VMC |
Weather Elements | Turbulence |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zmp.artcc |
Operator | general aviation : corporate |
Make Model Name | King Air C90 E90 |
Operating Under FAR Part | Part 91 |
Flight Phase | cruise : level |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : corporate |
Function | flight crew : captain oversight : pic |
Qualification | pilot : instrument pilot : multi engine pilot : commercial |
Experience | flight time last 90 days : 65 flight time total : 2250 flight time type : 350 |
ASRS Report | 714003 |
Events | |
Anomaly | altitude deviation : excursion from assigned altitude non adherence : clearance |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : returned to assigned altitude |
Supplementary | |
Problem Areas | Passenger Human Performance Aircraft Flight Crew Human Performance |
Primary Problem | Flight Crew Human Performance |
Narrative:
While flying in light to sometimes moderate turbulence (localized); a passenger that was sitting in right front seat (copilot's seat) was leaving seat to rejoin people in cabin. When he left the seat his pant leg caught the autoplt toggle on the pedestal and disconnected the autoplt. Altitude increased 200-300 ft in turbulence; and then I over-controled my correction resulting in a loss of about 800 ft; so getting to FL205 or so -- approximately 500 ft low! I immediately reestablished aircraft at correct altitude (FL210) and reengaged autoplt. There were no known conflicts; and ATC did not inquire as to the situation or to any altitude excursions. Of course; the entire situation would have been avoided had people not been moving about in the cockpit; and if I would have at least guarded the autoplt-flight director toggles with my hand; instead I was trying to help this person to get out of the seat. So; no more non-pilots in the cockpit; unless they agree to stay put for the entire flight; anyway.
Original NASA ASRS Text
Title: KING AIR PLT HAS AUTOPLT DISENGAGED BY PAX CLBING OUT OF THE COCKPIT.
Narrative: WHILE FLYING IN LIGHT TO SOMETIMES MODERATE TURB (LOCALIZED); A PAX THAT WAS SITTING IN R FRONT SEAT (COPLT'S SEAT) WAS LEAVING SEAT TO REJOIN PEOPLE IN CABIN. WHEN HE LEFT THE SEAT HIS PANT LEG CAUGHT THE AUTOPLT TOGGLE ON THE PEDESTAL AND DISCONNECTED THE AUTOPLT. ALT INCREASED 200-300 FT IN TURB; AND THEN I OVER-CTLED MY CORRECTION RESULTING IN A LOSS OF ABOUT 800 FT; SO GETTING TO FL205 OR SO -- APPROX 500 FT LOW! I IMMEDIATELY REESTABLISHED ACFT AT CORRECT ALT (FL210) AND REENGAGED AUTOPLT. THERE WERE NO KNOWN CONFLICTS; AND ATC DID NOT INQUIRE AS TO THE SITUATION OR TO ANY ALT EXCURSIONS. OF COURSE; THE ENTIRE SITUATION WOULD HAVE BEEN AVOIDED HAD PEOPLE NOT BEEN MOVING ABOUT IN THE COCKPIT; AND IF I WOULD HAVE AT LEAST GUARDED THE AUTOPLT-FLT DIRECTOR TOGGLES WITH MY HAND; INSTEAD I WAS TRYING TO HELP THIS PERSON TO GET OUT OF THE SEAT. SO; NO MORE NON-PLTS IN THE COCKPIT; UNLESS THEY AGREE TO STAY PUT FOR THE ENTIRE FLT; ANYWAY.
Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.