Narrative:

We were conducting a maximum gross weight takeoff from runway 17L in den. During the takeoff roll we aborted the takeoff due to a #2 engine fuel filter bypass light with master caution. Takeoff weight was 129.7 pounds; speeds were V1 163 KTS; vr 166 KTS; V2 170 KTS. Abort was initiated at approximately 130 KTS. We consulted the brake cooling chart and determined they were in the fuse plug melt zone. Maintenance was contacted and expressed their wishes that we taxi to the gate. Brakes were never set and all 4 tires deflated either approaching the gate or at gate. Dispatch and the flight office were notified. We were debriefed and removed from the trip.

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Original NASA ASRS Text

Title: B737 CREW ABORTS TKOF AT DEN FOR FUEL FILTER BYPASS WITH MASTER CAUTION.

Narrative: WE WERE CONDUCTING A MAX GROSS WT TKOF FROM RWY 17L IN DEN. DURING THE TKOF ROLL WE ABORTED THE TKOF DUE TO A #2 ENG FUEL FILTER BYPASS LIGHT WITH MASTER CAUTION. TKOF WT WAS 129.7 LBS; SPDS WERE V1 163 KTS; VR 166 KTS; V2 170 KTS. ABORT WAS INITIATED AT APPROX 130 KTS. WE CONSULTED THE BRAKE COOLING CHART AND DETERMINED THEY WERE IN THE FUSE PLUG MELT ZONE. MAINT WAS CONTACTED AND EXPRESSED THEIR WISHES THAT WE TAXI TO THE GATE. BRAKES WERE NEVER SET AND ALL 4 TIRES DEFLATED EITHER APCHING THE GATE OR AT GATE. DISPATCH AND THE FLT OFFICE WERE NOTIFIED. WE WERE DEBRIEFED AND REMOVED FROM THE TRIP.

Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.