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|
Attributes | |
ACN | 759114 |
Time | |
Date | 200710 |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : oak.airport |
State Reference | CA |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Dawn |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Widebody Transport |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : takeoff roll |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer oversight : pic |
Qualification | pilot : multi engine pilot : instrument pilot : commercial pilot : flight engineer |
Experience | flight time last 90 days : 143 flight time total : 6100 |
ASRS Report | 759114 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain |
Qualification | pilot : atp |
Experience | flight time last 90 days : 150 flight time total : 13300 flight time type : 4300 |
ASRS Report | 759115 |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : published procedure |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | flight crew : rejected takeoff |
Supplementary | |
Problem Areas | Flight Crew Human Performance Maintenance Human Performance |
Primary Problem | Flight Crew Human Performance |
Narrative:
We were cleared for takeoff runway 29 oakland. The first officer was flying and the captain set takeoff power. The autothrottles were MEL'ed inoperative. Upon setting takeoff power; the captain and first officer both noticed an inaccurate presentation of airspeed. We were receiving a digital readout; but the airspeed tapes never came down. The takeoff was rejected at 100 KTS. We returned to the oakland ramp. We were told the pitot tube covers were still on. Maintenance performed an adiru check and returned the aircraft to service. The first officer recalled seeing the pitot covers installed but forgot to inform maintenance of the discrepancy. We departed 1 hour later. When the pitot tube covers were discovered on the plane; no one was near the aircraft at that time. The first officer continued the walkaround intending to alert someone to this situation. This never happened and we ended up rejecting the takeoff. I feel that in the future; if anything like this is ever found; to find or call maintenance personnel immediately; stop the preflight and take care of this situation. Alert the captain right away and then complete the walkaround.
Original NASA ASRS Text
Title: WIDEBODY FREIGHT ACFT REJECTED TKOF FOR AIRSPEED ANOMALY. PITOT TUBE COVERS WERE STILL INSTALLED.
Narrative: WE WERE CLRED FOR TKOF RWY 29 OAKLAND. THE FO WAS FLYING AND THE CAPT SET TKOF PWR. THE AUTOTHROTTLES WERE MEL'ED INOP. UPON SETTING TKOF PWR; THE CAPT AND FO BOTH NOTICED AN INACCURATE PRESENTATION OF AIRSPD. WE WERE RECEIVING A DIGITAL READOUT; BUT THE AIRSPD TAPES NEVER CAME DOWN. THE TKOF WAS REJECTED AT 100 KTS. WE RETURNED TO THE OAKLAND RAMP. WE WERE TOLD THE PITOT TUBE COVERS WERE STILL ON. MAINT PERFORMED AN ADIRU CHK AND RETURNED THE ACFT TO SVC. THE FO RECALLED SEEING THE PITOT COVERS INSTALLED BUT FORGOT TO INFORM MAINT OF THE DISCREPANCY. WE DEPARTED 1 HR LATER. WHEN THE PITOT TUBE COVERS WERE DISCOVERED ON THE PLANE; NO ONE WAS NEAR THE ACFT AT THAT TIME. THE FO CONTINUED THE WALKAROUND INTENDING TO ALERT SOMEONE TO THIS SITUATION. THIS NEVER HAPPENED AND WE ENDED UP REJECTING THE TKOF. I FEEL THAT IN THE FUTURE; IF ANYTHING LIKE THIS IS EVER FOUND; TO FIND OR CALL MAINT PERSONNEL IMMEDIATELY; STOP THE PREFLT AND TAKE CARE OF THIS SITUATION. ALERT THE CAPT RIGHT AWAY AND THEN COMPLETE THE WALKAROUND.
Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.