37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 92878 |
Time | |
Date | 198808 |
Day | Fri |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | atc facility : ape |
State Reference | OH |
Altitude | msl bound lower : 25000 msl bound upper : 31000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zid tracon : cmh |
Operator | common carrier : air carrier |
Make Model Name | Large Transport, Low Wing, 3 Turbojet Eng |
Flight Phase | cruise other descent other |
Route In Use | approach : straight in arrival other enroute : direct |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 92878 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : second officer |
Qualification | pilot : commercial pilot : instrument pilot : flight engineer |
Experience | flight time last 90 days : 10 flight time total : 6000 flight time type : 1500 |
ASRS Report | 92976 |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : published procedure non adherence : far |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : overcame equipment problem none taken : detected after the fact |
Consequence | Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
Xfeeding could not be accomplished from tank #2 to engines #1 and #3. Second officer panel set up properly and all indications of valves and switches appeared normal--especially the #2 xfeed valve and associated blue valve in transit light which illuminated each time the switch was moved. We were compelled to dump from #2 to even the load and made an unscheduled stop at cmh, rather than continue on to mci (from lga). No emergency was declared. We were advised by company tech services that the in transit light is connected to the activator rather than the valve. It was found the valve itself was stuck but we nonetheless got a light each time the switch was moved. We believe that this situation is deceptive, dangerous and potentially lethal and should be corrected at once. Supplemental information from acn 92867: during this incident fuel was dumped while airborne. Flight crew failed to notify ATC that fuel was being dumped. Captain elected not to declare an emergency.
Original NASA ASRS Text
Title: ACR LGT UNSCHEDULED LNDG DUE TO FUEL CROSSFEED PROBLEM. PIC DUMPED FUEL WITHOUT NOTIFYING ATC.
Narrative: XFEEDING COULD NOT BE ACCOMPLISHED FROM TANK #2 TO ENGS #1 AND #3. S/O PANEL SET UP PROPERLY AND ALL INDICATIONS OF VALVES AND SWITCHES APPEARED NORMAL--ESPECIALLY THE #2 XFEED VALVE AND ASSOCIATED BLUE VALVE IN TRANSIT LIGHT WHICH ILLUMINATED EACH TIME THE SWITCH WAS MOVED. WE WERE COMPELLED TO DUMP FROM #2 TO EVEN THE LOAD AND MADE AN UNSCHEDULED STOP AT CMH, RATHER THAN CONTINUE ON TO MCI (FROM LGA). NO EMER WAS DECLARED. WE WERE ADVISED BY COMPANY TECH SVCS THAT THE IN TRANSIT LIGHT IS CONNECTED TO THE ACTIVATOR RATHER THAN THE VALVE. IT WAS FOUND THE VALVE ITSELF WAS STUCK BUT WE NONETHELESS GOT A LIGHT EACH TIME THE SWITCH WAS MOVED. WE BELIEVE THAT THIS SITUATION IS DECEPTIVE, DANGEROUS AND POTENTIALLY LETHAL AND SHOULD BE CORRECTED AT ONCE. SUPPLEMENTAL INFO FROM ACN 92867: DURING THIS INCIDENT FUEL WAS DUMPED WHILE AIRBORNE. FLT CREW FAILED TO NOTIFY ATC THAT FUEL WAS BEING DUMPED. CAPT ELECTED NOT TO DECLARE AN EMER.
Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.