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|
Attributes | |
ACN | 938802 |
Time | |
Date | 201103 |
Local Time Of Day | 0601-1200 |
Place | |
Locale Reference | ZZZ.Airport |
State Reference | US |
Environment | |
Light | Daylight |
Aircraft 1 | |
Make Model Name | MD-80 Series (DC-9-80) Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | Takeoff |
Flight Plan | IFR |
Component | |
Aircraft Component | Turbine Engine |
Person 1 | |
Function | First Officer Pilot Not Flying |
Person 2 | |
Function | Captain Pilot Flying |
Qualification | Flight Crew Air Transport Pilot (ATP) |
Events | |
Anomaly | Aircraft Equipment Problem Critical |
Narrative:
The aircraft had previously flown that day. A two engine taxi was used and engine anti-ice used due to the temperature and dew point spread. Aircraft weight was 147.3 for takeoff. Normal engine acceleration was observed; auto throttles engaged and aircraft accelerated normally. Simultaneously; at V1; we felt significant compressor stalls accompanied by EPR fluctuations on the right engine. The captain immediately aborted the takeoff as I called 'engine failure;' remaining and stopping on centerline of runway. We notified the tower of our abort and our intention to evaluate the situation on the runway.after noting normal engine parameters and brake temperatures; we advised the tower that we could taxi clear of runway. Once we taxied clear; an announcement to the passengers was made; and then a cabin evaluation was requested of the flight attendants. The flight attendants advised no issues in the cabin. Further evaluation of the engine issue revealed no throttle response from the right engine; but it had normal idle indications and no vibrations were observed. Engine was secured and shutdown normally. The company was notified and a gate was requested. Brake temperatures were monitored and ATC cleared us to the gate. Company was notified to remain clear of main gear. Brakes began cooling during long slow taxi to gate. No emergency was declared.
Original NASA ASRS Text
Title: An MD80 flight crew rejected their takeoff at V1 upon experiencing compressor stalls on the right engine.
Narrative: The aircraft had previously flown that day. A two engine taxi was used and engine anti-ice used due to the temperature and dew point spread. Aircraft weight was 147.3 for takeoff. Normal engine acceleration was observed; auto throttles engaged and aircraft accelerated normally. Simultaneously; at V1; we felt significant compressor stalls accompanied by EPR fluctuations on the right engine. The Captain immediately aborted the takeoff as I called 'engine failure;' remaining and stopping on centerline of runway. We notified the Tower of our abort and our intention to evaluate the situation on the runway.After noting normal engine parameters and brake temperatures; we advised the tower that we could taxi clear of runway. Once we taxied clear; an announcement to the passengers was made; and then a cabin evaluation was requested of the flight attendants. The Flight Attendants advised no issues in the cabin. Further evaluation of the engine issue revealed no throttle response from the right engine; but it had normal idle indications and no vibrations were observed. Engine was secured and shutdown normally. The company was notified and a gate was requested. Brake temperatures were monitored and ATC cleared us to the gate. Company was notified to remain clear of main gear. Brakes began cooling during long slow taxi to gate. No emergency was declared.
Data retrieved from NASA's ASRS site as of April 2012 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.