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|
Attributes | |
ACN | 94739 |
Time | |
Date | 198809 |
Day | Sun |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : apa |
State Reference | CO |
Altitude | msl bound lower : 5600 msl bound upper : 6600 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tower : apa tower : rno |
Operator | general aviation : corporate |
Make Model Name | Small Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | climbout : takeoff ground other : taxi landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : captain oversight : pic |
Qualification | pilot : commercial pilot : instrument pilot : atp |
Experience | flight time last 90 days : 180 flight time total : 6700 |
ASRS Report | 94739 |
Person 2 | |
Affiliation | Other |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | non adherence : far other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | other |
Consequence | faa : reviewed incident with flight crew other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
Aircraft was parked inside hangar overnight at a large national FBO. I ordered the aircraft to be pulled out of the hangar and readied for flight at approximately XA00 local time. Plane was pulled out and had coffee and ice put in, and was presumed ready to fly. Plane was placed at far side of ramp where there was no light from the bldg. I arrived at airport, walked around aircraft, removed engine plugs, removed chock from main gear of aircraft, locked the nose baggage compartments and never saw the tow bar which was painted dark blue and blended into the dark ramp. I taxied out and never felt or heard the tow bar on the nose gear until lift off, when I heard a loud thump and felt a shudder. I presumed that I had blown a nose tire on lift off and returned immediately to a landing. Upon T/D the aircraft immediately veered sharply to the right and I used full differential braking to keep the aircraft straight on the runway. Upon shutdown, I discovered that the tow bar was still attached to the nose gear. Damage consisted only of 6 broken shear bolts in the nose steering collar. It could have been worse.
Original NASA ASRS Text
Title: TKOF WITH NOSE TOW BAR STILL ATTACHED.
Narrative: ACFT WAS PARKED INSIDE HANGAR OVERNIGHT AT A LARGE NATL FBO. I ORDERED THE ACFT TO BE PULLED OUT OF THE HANGAR AND READIED FOR FLT AT APPROX XA00 LCL TIME. PLANE WAS PULLED OUT AND HAD COFFEE AND ICE PUT IN, AND WAS PRESUMED READY TO FLY. PLANE WAS PLACED AT FAR SIDE OF RAMP WHERE THERE WAS NO LIGHT FROM THE BLDG. I ARRIVED AT ARPT, WALKED AROUND ACFT, REMOVED ENG PLUGS, REMOVED CHOCK FROM MAIN GEAR OF ACFT, LOCKED THE NOSE BAGGAGE COMPARTMENTS AND NEVER SAW THE TOW BAR WHICH WAS PAINTED DARK BLUE AND BLENDED INTO THE DARK RAMP. I TAXIED OUT AND NEVER FELT OR HEARD THE TOW BAR ON THE NOSE GEAR UNTIL LIFT OFF, WHEN I HEARD A LOUD THUMP AND FELT A SHUDDER. I PRESUMED THAT I HAD BLOWN A NOSE TIRE ON LIFT OFF AND RETURNED IMMEDIATELY TO A LNDG. UPON T/D THE ACFT IMMEDIATELY VEERED SHARPLY TO THE RIGHT AND I USED FULL DIFFERENTIAL BRAKING TO KEEP THE ACFT STRAIGHT ON THE RWY. UPON SHUTDOWN, I DISCOVERED THAT THE TOW BAR WAS STILL ATTACHED TO THE NOSE GEAR. DAMAGE CONSISTED ONLY OF 6 BROKEN SHEAR BOLTS IN THE NOSE STEERING COLLAR. IT COULD HAVE BEEN WORSE.
Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.