37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 965983 |
Time | |
Date | 201108 |
Local Time Of Day | 1201-1800 |
Place | |
Locale Reference | ZZZ.Airport |
State Reference | US |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Make Model Name | MD-80 Series (DC-9-80) Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | Climb |
Flight Plan | IFR |
Component | |
Aircraft Component | Air/Ground Communication |
Person 1 | |
Function | First Officer |
Person 2 | |
Function | Captain |
Qualification | Flight Crew Air Transport Pilot (ATP) |
Events | |
Anomaly | Aircraft Equipment Problem Critical Deviation - Altitude Excursion From Assigned Altitude Flight Deck / Cabin / Aircraft Event Smoke / Fire / Fumes / Odor Inflight Event / Encounter Weather / Turbulence |
Narrative:
The aircraft came with a write-up; 'electrical fumes reported in cabin when engine/airfoil ice was turned on.' maintenance could not duplicate and signed off the logbook entry. Flight was delayed due to a different maintenance problem. The problem was a hydraulic leak discovered by the ramp crew just prior to departure from the gate. That problem was fixed and flight departed approximately 90 minutes late. The rest of the flight was uneventful. During climb from FL320 to FL360 [in our next flight]; we were in IMC and light to moderate rain showers. We encountered icing conditions passing approximately FL330. Shortly after the engine and wing anti-ice was turned on; a strong electrical burning odor became apparent in the cabin and the cockpit. The flight attendants called the cockpit to report the fumes and we acknowledged same. The anti-ice was turned off and the burning smell began to dissipate. At this point we elected to level the aircraft at FL330. Within seconds of leveling the aircraft; both engines began to compressor stall. We immediately disconnected the auto-throttles and reduced power. The engine heat and ignition was turned back on which stopped the compressor stall. At this point we attempted to contact ATC for a lower altitude; but the radio antennae had apparently picked up so much ice in a very short time that we could not hear ATC on either radio; static only. We were also dodging thunderstorms at this point. '7700' was selected on the transponder and we continued a descent to a lower; warmer altitude so that the engine anti-ice could be turned off. Upon reaching FL180 we were able to turn engine anti-ice off again and the electrical burning odor subsided. Once the communications were restored; we confirmed the emergency declaration and diverted. The visual approach and landing were uneventful. After clearing the runway; the aircraft was inspected by arff; [who] reported no apparent damage to the aircraft. The subsequent taxi in to the gate was uneventful.
Original NASA ASRS Text
Title: An air carrier crew reported that when the wing and engine anti-ice were turned ON while climbing IMC; electrical fumes were detected throughout the aircraft; so an emergency was declared and the flight diverted to a nearby airport.
Narrative: The aircraft came with a write-up; 'Electrical fumes reported in cabin when engine/airfoil ice was turned on.' Maintenance could not duplicate and signed off the logbook entry. Flight was delayed due to a different maintenance problem. The problem was a hydraulic leak discovered by the ramp crew just prior to departure from the gate. That problem was fixed and flight departed approximately 90 minutes late. The rest of the flight was uneventful. During climb from FL320 to FL360 [in our next flight]; we were in IMC and light to moderate rain showers. We encountered icing conditions passing approximately FL330. Shortly after the engine and wing anti-ice was turned on; a strong electrical burning odor became apparent in the cabin and the cockpit. The flight attendants called the cockpit to report the fumes and we acknowledged same. The anti-ice was turned off and the burning smell began to dissipate. At this point we elected to level the aircraft at FL330. Within seconds of leveling the aircraft; both engines began to compressor stall. We immediately disconnected the auto-throttles and reduced power. The engine heat and ignition was turned back on which stopped the compressor stall. At this point we attempted to contact ATC for a lower altitude; but the radio antennae had apparently picked up so much ice in a very short time that we could not hear ATC on either radio; static only. We were also dodging thunderstorms at this point. '7700' was selected on the transponder and we continued a descent to a lower; warmer altitude so that the engine anti-ice could be turned off. Upon reaching FL180 we were able to turn engine anti-ice off again and the electrical burning odor subsided. Once the communications were restored; we confirmed the emergency declaration and diverted. The visual approach and landing were uneventful. After clearing the runway; the aircraft was inspected by ARFF; [who] reported no apparent damage to the aircraft. The subsequent taxi in to the gate was uneventful.
Data retrieved from NASA's ASRS site as of April 2012 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.