37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 1031166 |
Time | |
Date | 201208 |
Local Time Of Day | 1201-1800 |
Place | |
Locale Reference | ZZZ.ARTCC |
State Reference | US |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Make Model Name | Citation II S2/Bravo (C550) |
Operating Under FAR Part | Part 91 |
Flight Phase | Cruise |
Route In Use | Direct |
Flight Plan | IFR |
Component | |
Aircraft Component | Pressurization Outflow Valve |
Person 1 | |
Function | Pilot Flying Single Pilot |
Qualification | Flight Crew Instrument Flight Crew Multiengine Flight Crew Air Transport Pilot (ATP) |
Experience | Flight Crew Last 90 Days 100 Flight Crew Total 8500 Flight Crew Type 2000 |
Events | |
Anomaly | Aircraft Equipment Problem Critical |
Narrative:
The aircraft was level at FL370 for over an hour. A rather loud whistling noise was heard. I observed the cabin climb rate jump from 0 to +3;000 FPM. We were experiencing a rapid depressurization. I declared an emergency with center and requested an immediate descent. We began a descent immediately. Center was very helpful in giving me directions to various airports. Oxygen masks were donned by pilot and passengers; passengers were briefed; and we made a course reversal toward [nearest suitable airport]. As we proceeded; we leveled the aircraft at 14;000 ft with ATC approval. At that point; the cabin was holding at 3;000 ft. Oxygen masks were removed. The emergency status was canceled. I told ATC that we no longer needed priority handling and that we could be sequenced onto an arrival and an approach normally. We changed our destination as we considered maintenance availability at various airports. The approach and landing were normal. There were (to my knowledge) no conflicts with other aircraft. Center personnel responded promptly to all of our requests. I never heard any transmissions that would indicate that our situation/actions affected other aircraft (no heading or altitude changes were given). The emergency was handled promptly; professionally; and decisively by both myself and ATC personnel. Maintenance was performed [and] it was discovered that the right-hand pressurization check valve had failed. Instead of air being sent into the cabin to pressurize the aircraft and inflate the door seal; the air was allowed to escape into the right-hand nacelle. The flight resumed two days later.
Original NASA ASRS Text
Title: C-550 Captain (single pilot) reported loss of pressurization at FL370. Emergency was declared; a descent executed; and a diversion to an appropriate airport followed; where a pressurization check valve was found to have failed.
Narrative: The aircraft was level at FL370 for over an hour. A rather loud whistling noise was heard. I observed the cabin climb rate jump from 0 to +3;000 FPM. We were experiencing a rapid depressurization. I declared an emergency with Center and requested an immediate descent. We began a descent immediately. Center was very helpful in giving me directions to various airports. Oxygen masks were donned by pilot and passengers; passengers were briefed; and we made a course reversal toward [nearest suitable airport]. As we proceeded; we leveled the aircraft at 14;000 FT with ATC approval. At that point; the cabin was holding at 3;000 FT. Oxygen masks were removed. The emergency status was canceled. I told ATC that we no longer needed priority handling and that we could be sequenced onto an arrival and an approach normally. We changed our destination as we considered maintenance availability at various airports. The approach and landing were normal. There were (to my knowledge) no conflicts with other aircraft. Center personnel responded promptly to all of our requests. I never heard any transmissions that would indicate that our situation/actions affected other aircraft (no heading or altitude changes were given). The emergency was handled promptly; professionally; and decisively by both myself and ATC personnel. Maintenance was performed [and] it was discovered that the right-hand pressurization check valve had failed. Instead of air being sent into the cabin to pressurize the aircraft and inflate the door seal; the air was allowed to escape into the right-hand nacelle. The flight resumed two days later.
Data retrieved from NASA's ASRS site as of July 2013 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.