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|
Attributes | |
ACN | 132592 |
Time | |
Date | 199001 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : geg |
State Reference | WA |
Altitude | msl bound lower : 4000 msl bound upper : 4000 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : geg tower : bna |
Operator | common carrier : air carrier |
Make Model Name | Large Transport, Low Wing, 3 Turbojet Eng |
Flight Phase | descent : approach |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 200 flight time total : 18000 flight time type : 8000 |
ASRS Report | 132592 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other other : unspecified |
Resolutory Action | flight crew : declared emergency flight crew : overcame equipment problem |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
On descent into geg, approximately 15 mi from T/D, a F/a called on the interphone and advised us of a fire in the aft left lav. The second officer immediately went back to assess the situation. He discovered the smoke was coming from the toilet bowl. He discharged a halon fire extinguisher into the toilet bowl and reported to us the smoke had subsided just prior to landing in spokane. It was later discovered the toilet flush motor had malfunctioned and overheated, causing the smoke. It was the spokane fire marshall that discovered the source of the smoke after we parked the aircraft at the gate and deplaned the passenger. During this entire time the flush motor circuit breaker in the cockpit did not pop and the smoke detector in the lav apparently did not chime until after the halon fire extinguisher had been discharged in the lav. In this instance the problem terminated west/O any injury or loss of life, but one can imagine how serious an incident of this kind could have been if the materials in that area had erupted into flames.
Original NASA ASRS Text
Title: ACR LGT EXPERIENCES LAVATORY FIRE SHORTLY BEFORE LNDG.
Narrative: ON DSCNT INTO GEG, APPROX 15 MI FROM T/D, A F/A CALLED ON THE INTERPHONE AND ADVISED US OF A FIRE IN THE AFT LEFT LAV. THE S/O IMMEDIATELY WENT BACK TO ASSESS THE SITUATION. HE DISCOVERED THE SMOKE WAS COMING FROM THE TOILET BOWL. HE DISCHARGED A HALON FIRE EXTINGUISHER INTO THE TOILET BOWL AND RPTED TO US THE SMOKE HAD SUBSIDED JUST PRIOR TO LNDG IN SPOKANE. IT WAS LATER DISCOVERED THE TOILET FLUSH MOTOR HAD MALFUNCTIONED AND OVERHEATED, CAUSING THE SMOKE. IT WAS THE SPOKANE FIRE MARSHALL THAT DISCOVERED THE SOURCE OF THE SMOKE AFTER WE PARKED THE ACFT AT THE GATE AND DEPLANED THE PAX. DURING THIS ENTIRE TIME THE FLUSH MOTOR CB IN THE COCKPIT DID NOT POP AND THE SMOKE DETECTOR IN THE LAV APPARENTLY DID NOT CHIME UNTIL AFTER THE HALON FIRE EXTINGUISHER HAD BEEN DISCHARGED IN THE LAV. IN THIS INSTANCE THE PROB TERMINATED W/O ANY INJURY OR LOSS OF LIFE, BUT ONE CAN IMAGINE HOW SERIOUS AN INCIDENT OF THIS KIND COULD HAVE BEEN IF THE MATERIALS IN THAT AREA HAD ERUPTED INTO FLAMES.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.