37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 134261 |
Time | |
Date | 199001 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : buf |
State Reference | NY |
Altitude | msl bound lower : 19000 msl bound upper : 19000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zob artcc : zoa |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Navigation In Use | Other |
Flight Phase | cruise other cruise other other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time total : 8200 flight time type : 1200 |
ASRS Report | 134261 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | controller : issued new clearance flight crew : declared emergency flight crew : overcame equipment problem other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
At FL190 35 NM from buf loud buzzing was heard. Electrical system shutdown and smoke filled the cockpit. Electrical system came back on line with left generator off light illuminated. Checklist was accomplished, smoke subsided, and an emergency was declared with a requested return to buf. Buf WX was approximately 25 ovc 10 using runway 23. An expeditious descent and ILS runway 23 was accomplished. Equipment was requested to stand by. An uneventful landing was made. Smoke increased slightly as aircraft approached the gate. So cockpit windows were opened, aircraft power was shut down at the gate with exit lights on. Passenger were directed to leave aircraft without baggage. Equipment was requested to approach the aircraft and check for any remaining fire.
Original NASA ASRS Text
Title: ELECTRICAL FIRE AND SMOKE IN COCKPIT OF MLG.
Narrative: AT FL190 35 NM FROM BUF LOUD BUZZING WAS HEARD. ELECTRICAL SYSTEM SHUTDOWN AND SMOKE FILLED THE COCKPIT. ELECTRICAL SYSTEM CAME BACK ON LINE WITH LEFT GENERATOR OFF LIGHT ILLUMINATED. CHECKLIST WAS ACCOMPLISHED, SMOKE SUBSIDED, AND AN EMER WAS DECLARED WITH A REQUESTED RETURN TO BUF. BUF WX WAS APPROX 25 OVC 10 USING RWY 23. AN EXPEDITIOUS DSCNT AND ILS RWY 23 WAS ACCOMPLISHED. EQUIPMENT WAS REQUESTED TO STAND BY. AN UNEVENTFUL LNDG WAS MADE. SMOKE INCREASED SLIGHTLY AS ACFT APCHED THE GATE. SO COCKPIT WINDOWS WERE OPENED, ACFT POWER WAS SHUT DOWN AT THE GATE WITH EXIT LIGHTS ON. PAX WERE DIRECTED TO LEAVE ACFT WITHOUT BAGGAGE. EQUIPMENT WAS REQUESTED TO APCH THE ACFT AND CHECK FOR ANY REMAINING FIRE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.