37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 1394633 |
Time | |
Date | 201610 |
Local Time Of Day | 1801-2400 |
Place | |
Locale Reference | ZZZ.Airport |
State Reference | US |
Environment | |
Flight Conditions | VMC |
Aircraft 1 | |
Make Model Name | B737 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | Climb |
Flight Plan | IFR |
Component | |
Aircraft Component | Turbine Engine |
Person 1 | |
Function | Pilot Flying Captain |
Qualification | Flight Crew Air Transport Pilot (ATP) |
Experience | Flight Crew Last 90 Days 200 Flight Crew Total 20000 Flight Crew Type 1500 |
Person 2 | |
Function | First Officer Pilot Not Flying |
Qualification | Flight Crew Air Transport Pilot (ATP) |
Experience | Flight Crew Last 90 Days 143 Flight Crew Total 15750 Flight Crew Type 2500 |
Events | |
Anomaly | Aircraft Equipment Problem Less Severe Inflight Event / Encounter Bird / Animal |
Narrative:
Approximately 500 feet (after gear retraction but prior to flap retraction) jolt/yaw accompanied by bang similar to those experienced in simulator (associated with severe damage). I was hand flying (and focused on that) and by the time I looked at the engine instruments; all appeared normal. At the same time a strong burning smell was experienced. We quickly decided to return and not continue. We communicated with departure and stated our intentions. A few minutes after the odor started; it began to dissipate. ATC gave us a heading and assigned 9000 as an altitude. I engaged the autopilot (after the first officer reminded me it was available). The first officer ran the after takeoff checklist as well as set up the box for the return. I called the flight attendants and informed them of our situation. They informed me that they saw torching in the left engine when the bang occurred. The first officer and I concluded that we most likely ingested a bird into the left engine and that the engine had a compressor stall. I sent a message to dispatch informing them of our condition and intent to return. Dispatch requested the emergency equipment for us. The first officer and I discussed our landing overweight; and continued back for an uneventful landing (overweight).
Original NASA ASRS Text
Title: B737 flight crew reported a bird strike below 1;000 feet on departure which caused a momentary compressor stall before resuming normal operation. Flight returns to the departure airport for an overweight landing.
Narrative: Approximately 500 feet (after gear retraction but prior to flap retraction) jolt/yaw accompanied by bang similar to those experienced in simulator (associated with severe damage). I was hand flying (and focused on that) and by the time I looked at the engine instruments; all appeared normal. At the same time a strong burning smell was experienced. We quickly decided to return and not continue. We communicated with departure and stated our intentions. A few minutes after the odor started; it began to dissipate. ATC gave us a heading and assigned 9000 as an altitude. I engaged the autopilot (after the FO reminded me it was available). The FO ran the after takeoff checklist as well as set up the box for the return. I called the flight attendants and informed them of our situation. They informed me that they saw torching in the left engine when the bang occurred. The FO and I concluded that we most likely ingested a bird into the left engine and that the engine had a compressor stall. I sent a message to dispatch informing them of our condition and intent to return. Dispatch requested the emergency equipment for us. The FO and I discussed our landing overweight; and continued back for an uneventful landing (overweight).
Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.