Narrative:

Approximately 500 feet (after gear retraction but prior to flap retraction) jolt/yaw accompanied by bang similar to those experienced in simulator (associated with severe damage). I was hand flying (and focused on that) and by the time I looked at the engine instruments; all appeared normal. At the same time a strong burning smell was experienced. We quickly decided to return and not continue. We communicated with departure and stated our intentions. A few minutes after the odor started; it began to dissipate. ATC gave us a heading and assigned 9000 as an altitude. I engaged the autopilot (after the first officer reminded me it was available). The first officer ran the after takeoff checklist as well as set up the box for the return. I called the flight attendants and informed them of our situation. They informed me that they saw torching in the left engine when the bang occurred. The first officer and I concluded that we most likely ingested a bird into the left engine and that the engine had a compressor stall. I sent a message to dispatch informing them of our condition and intent to return. Dispatch requested the emergency equipment for us. The first officer and I discussed our landing overweight; and continued back for an uneventful landing (overweight).

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Original NASA ASRS Text

Title: B737 flight crew reported a bird strike below 1;000 feet on departure which caused a momentary compressor stall before resuming normal operation. Flight returns to the departure airport for an overweight landing.

Narrative: Approximately 500 feet (after gear retraction but prior to flap retraction) jolt/yaw accompanied by bang similar to those experienced in simulator (associated with severe damage). I was hand flying (and focused on that) and by the time I looked at the engine instruments; all appeared normal. At the same time a strong burning smell was experienced. We quickly decided to return and not continue. We communicated with departure and stated our intentions. A few minutes after the odor started; it began to dissipate. ATC gave us a heading and assigned 9000 as an altitude. I engaged the autopilot (after the FO reminded me it was available). The FO ran the after takeoff checklist as well as set up the box for the return. I called the flight attendants and informed them of our situation. They informed me that they saw torching in the left engine when the bang occurred. The FO and I concluded that we most likely ingested a bird into the left engine and that the engine had a compressor stall. I sent a message to dispatch informing them of our condition and intent to return. Dispatch requested the emergency equipment for us. The FO and I discussed our landing overweight; and continued back for an uneventful landing (overweight).

Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.