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Attributes | |
ACN | 150643 |
Time | |
Date | 199007 |
Day | Thu |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : bos |
State Reference | MA |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : flight engineer pilot : atp pilot : cfi pilot : instrument |
Experience | flight time last 90 days : 150 flight time total : 7000 flight time type : 300 |
ASRS Report | 150643 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other controllera other flight crewa |
Resolutory Action | flight crew : declared emergency none taken : unable other |
Consequence | other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Performed a normal landing in boston with a medium large transport. After a soft T/D the thrust reversers failed to deploy. Tower advised us that smoke was coming from main tires. We exited runway and came to a stop. There was no apparent directional control problem so we elected to clear the highspd taxiway and taxied onto runway 22, which was not active at the time. Tower advised us that the smoke had stopped and fire equipment was on the way. We ended up deplaning the passengers and F/as on runway 22 and busing them to the gate. Maintenance then towed the aircraft to the gate. It would appear that the anti-skid failed on the main tires #2 and #4 and caused them to blow. The aft F/a stated that she heard 2 loud pops after T/D. That was probably when I applied the brakes. Aircraft had previous write up in logbook stating that 1 tire blew on landing in charlotte, nc, and the thrust reversers did not work on landing. I believe this airplane needs to have a good looksee by maintenance to see where the problem is. Runway was dry and airport was VFR.
Original NASA ASRS Text
Title: ACR MLG BLEW TWO TIRES LNDG AT BOS.
Narrative: PERFORMED A NORMAL LNDG IN BOSTON WITH A MLG. AFTER A SOFT T/D THE THRUST REVERSERS FAILED TO DEPLOY. TWR ADVISED US THAT SMOKE WAS COMING FROM MAIN TIRES. WE EXITED RWY AND CAME TO A STOP. THERE WAS NO APPARENT DIRECTIONAL CTL PROB SO WE ELECTED TO CLR THE HIGHSPD TXWY AND TAXIED ONTO RWY 22, WHICH WAS NOT ACTIVE AT THE TIME. TWR ADVISED US THAT THE SMOKE HAD STOPPED AND FIRE EQUIP WAS ON THE WAY. WE ENDED UP DEPLANING THE PAXS AND F/AS ON RWY 22 AND BUSING THEM TO THE GATE. MAINT THEN TOWED THE ACFT TO THE GATE. IT WOULD APPEAR THAT THE ANTI-SKID FAILED ON THE MAIN TIRES #2 AND #4 AND CAUSED THEM TO BLOW. THE AFT F/A STATED THAT SHE HEARD 2 LOUD POPS AFTER T/D. THAT WAS PROBABLY WHEN I APPLIED THE BRAKES. ACFT HAD PREVIOUS WRITE UP IN LOGBOOK STATING THAT 1 TIRE BLEW ON LNDG IN CHARLOTTE, NC, AND THE THRUST REVERSERS DID NOT WORK ON LNDG. I BELIEVE THIS AIRPLANE NEEDS TO HAVE A GOOD LOOKSEE BY MAINT TO SEE WHERE THE PROB IS. RWY WAS DRY AND ARPT WAS VFR.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.