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|
Attributes | |
ACN | 152286 |
Time | |
Date | 199007 |
Day | Sun |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : bff |
State Reference | NE |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | general aviation : personal |
Make Model Name | Small Aircraft, Low Wing, 1 Eng, Retractable Gear |
Flight Phase | landing other |
Flight Plan | None |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : private pilot : instrument |
Experience | flight time last 90 days : 38 flight time total : 852 flight time type : 71 |
ASRS Report | 152286 |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : published procedure other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | none taken : detected after the fact |
Consequence | other other Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
I woke up early and went to airport. Did run-up and hand a magnetic drop. Waited 4 hours for mechanic to replace plug. Departed airport tired and upset. 10 mins out of scotts bluff noticed cowling on engine loose. Made 180 degree turn and returned to scotts bluff to fasten cowling. I slowed to reduce speed to lower landing gear but had calls of other aircraft in vicinity of airport. Never got back to lower gear and because of aircraft activity forgot to rechk gump. Landed gear up, flaps down. Fatigue, distraction and frustration were the factors causing event. The best course to have taken was not to fly, because of the fatigue and being upset caused by the spark plug event, and waiting for mechanic.
Original NASA ASRS Text
Title: GEAR UP LNDG.
Narrative: I WOKE UP EARLY AND WENT TO ARPT. DID RUN-UP AND HAND A MAG DROP. WAITED 4 HRS FOR MECH TO REPLACE PLUG. DEPARTED ARPT TIRED AND UPSET. 10 MINS OUT OF SCOTTS BLUFF NOTICED COWLING ON ENG LOOSE. MADE 180 DEG TURN AND RETURNED TO SCOTTS BLUFF TO FASTEN COWLING. I SLOWED TO REDUCE SPD TO LOWER LNDG GEAR BUT HAD CALLS OF OTHER ACFT IN VICINITY OF ARPT. NEVER GOT BACK TO LOWER GEAR AND BECAUSE OF ACFT ACTIVITY FORGOT TO RECHK GUMP. LANDED GEAR UP, FLAPS DOWN. FATIGUE, DISTR AND FRUSTRATION WERE THE FACTORS CAUSING EVENT. THE BEST COURSE TO HAVE TAKEN WAS NOT TO FLY, BECAUSE OF THE FATIGUE AND BEING UPSET CAUSED BY THE SPARK PLUG EVENT, AND WAITING FOR MECH.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.