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|
Attributes | |
ACN | 152745 |
Time | |
Date | 199008 |
Day | Wed |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : msp |
State Reference | MN |
Altitude | agl bound lower : 0 agl bound upper : 1500 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : msp tower : msp |
Operator | common carrier : air carrier |
Make Model Name | Light Transport, Low Wing, 2 Turboprop Eng |
Flight Phase | descent other landing other other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 225 flight time total : 3865 |
ASRS Report | 152745 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : unspecified |
Resolutory Action | flight crew : overcame equipment problem flight crew : declared emergency |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
On the final approach into msp I selected gear down and it stopped halfway with the in transit lights on. Checked the hydraulic system only to find both engine driven pumps indicating zero psi. We executed a go around and completed the manual gear extension as per crew manual checklists. This was successful and we returned and landed on the long runway with crash fire rescue equipment standing by with no further incident. I had crash fire rescue equipment follow me to the gate because my steering and braking effectiveness was limited. Ironically, this same incident happened to me in 7/90 in a different aircraft. (Same type). In both cases, the hydraulic system sprung a leak resulting in the loss of main system pressure. Manual gear extension was successful in both cases.
Original NASA ASRS Text
Title: COMMUTER LTT LOST MAIN HYDRAULIC PRESSURE ENROUTE TO MSP. PROBLEM DISCOVERED WHEN GEAR WOULD NOT LOCK DOWN. MANUAL GEAR EXTENSION WAS SUCCESSFUL.
Narrative: ON THE FINAL APCH INTO MSP I SELECTED GEAR DOWN AND IT STOPPED HALFWAY WITH THE IN TRANSIT LIGHTS ON. CHKED THE HYD SYS ONLY TO FIND BOTH ENG DRIVEN PUMPS INDICATING ZERO PSI. WE EXECUTED A GO AROUND AND COMPLETED THE MANUAL GEAR EXTENSION AS PER CREW MANUAL CHKLISTS. THIS WAS SUCCESSFUL AND WE RETURNED AND LANDED ON THE LONG RWY WITH CFR STANDING BY WITH NO FURTHER INCIDENT. I HAD CFR FOLLOW ME TO THE GATE BECAUSE MY STEERING AND BRAKING EFFECTIVENESS WAS LIMITED. IRONICALLY, THIS SAME INCIDENT HAPPENED TO ME IN 7/90 IN A DIFFERENT ACFT. (SAME TYPE). IN BOTH CASES, THE HYD SYS SPRUNG A LEAK RESULTING IN THE LOSS OF MAIN SYS PRESSURE. MANUAL GEAR EXTENSION WAS SUCCESSFUL IN BOTH CASES.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.