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|
Attributes | |
ACN | 161793 |
Time | |
Date | 199011 |
Day | Sun |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : iah |
State Reference | TX |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tracon : fay |
Operator | common carrier : air carrier |
Make Model Name | Light Transport, Low Wing, 2 Turboprop Eng |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 260 flight time total : 3200 |
ASRS Report | 161793 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | non adherence : far non adherence : published procedure other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | none taken : unable |
Consequence | Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
Takeoff was aborted when right propeller RPM remained low. Aircraft returned to ramp. During parking checklist right electric feather switch was discovered in the on position. The aborted takeoff was logged in log book, switch was turned off, right engine was run up while maintenance personnel observed. Right engine opps checked ok and log book was signed off by maintenance. Aircraft continued on to destination. Factors contributing to occurrence were: nighttime, dark cockpit, unlit electric feather switch. Aircraft received line check prior to this flight by maintenance. Maintenance tried to flatten propeller pitch after line check due windy conditions, forgetting to turn off electric feather switch. Checklist does not address this switch or system except on first flight of the day.
Original NASA ASRS Text
Title: COMMUTER LTT TKOF ABORT BECAUSE 1 PROPELLER WOULD NOT SPIN UP. AFTER RETURN TO BLOCKS THE FEATHER SWITCH WAS FOUND IN THE ON POSITION.
Narrative: TKOF WAS ABORTED WHEN RIGHT PROP RPM REMAINED LOW. ACFT RETURNED TO RAMP. DURING PARKING CHKLIST RIGHT ELECTRIC FEATHER SWITCH WAS DISCOVERED IN THE ON POS. THE ABORTED TKOF WAS LOGGED IN LOG BOOK, SWITCH WAS TURNED OFF, RIGHT ENG WAS RUN UP WHILE MAINT PERSONNEL OBSERVED. RIGHT ENG OPPS CHKED OK AND LOG BOOK WAS SIGNED OFF BY MAINT. ACFT CONTINUED ON TO DEST. FACTORS CONTRIBUTING TO OCCURRENCE WERE: NIGHTTIME, DARK COCKPIT, UNLIT ELECTRIC FEATHER SWITCH. ACFT RECEIVED LINE CHK PRIOR TO THIS FLT BY MAINT. MAINT TRIED TO FLATTEN PROP PITCH AFTER LINE CHK DUE WINDY CONDITIONS, FORGETTING TO TURN OFF ELECTRIC FEATHER SWITCH. CHKLIST DOES NOT ADDRESS THIS SWITCH OR SYS EXCEPT ON FIRST FLT OF THE DAY.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.