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|
Attributes | |
ACN | 161891 |
Time | |
Date | 199010 |
Day | Wed |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : lax |
State Reference | CA |
Altitude | msl bound lower : 11000 msl bound upper : 11000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zla tracon : lax |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | climbout : intermediate altitude |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : cfi pilot : instrument pilot : commercial pilot : atp |
Experience | flight time last 90 days : 160 flight time total : 3700 flight time type : 200 |
ASRS Report | 161891 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : overcame equipment problem flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
We were climbing through 10000' when there was a series of loud banging sounds and a slight, ctlable yawing. The aircraft (an medium large transport) was leveled off at 11000'. The captain brought the #1 engine to flight idle, which seemed to make the banging stop. Both the captain and I felt that sounds were compressor stalls. The captain declared an emergency, elected to keep the #1 engine running, and a return to lax was started. The captain assigned me to fly the aircraft while he handled all the PNF duties. To my knowledge all checklists were complied with and no far's were violated! All ATC instructions were complied with in light of the emergency. An uneventful landing on runway 24L was made. As we cleared the runway, the #1 engine was shutdown and a single taxi made to the gate. The cause of the engine failure was found to be a bearing failure. My thanks to the captain for a job well done from the left seat.
Original NASA ASRS Text
Title: ACR MLG ENGINE FAILURE DURING CLIMB THROUGH 10000' RETURN LAND.
Narrative: WE WERE CLBING THROUGH 10000' WHEN THERE WAS A SERIES OF LOUD BANGING SOUNDS AND A SLIGHT, CTLABLE YAWING. THE ACFT (AN MLG) WAS LEVELED OFF AT 11000'. THE CAPT BROUGHT THE #1 ENG TO FLT IDLE, WHICH SEEMED TO MAKE THE BANGING STOP. BOTH THE CAPT AND I FELT THAT SOUNDS WERE COMPRESSOR STALLS. THE CAPT DECLARED AN EMER, ELECTED TO KEEP THE #1 ENG RUNNING, AND A RETURN TO LAX WAS STARTED. THE CAPT ASSIGNED ME TO FLY THE ACFT WHILE HE HANDLED ALL THE PNF DUTIES. TO MY KNOWLEDGE ALL CHKLISTS WERE COMPLIED WITH AND NO FAR'S WERE VIOLATED! ALL ATC INSTRUCTIONS WERE COMPLIED WITH IN LIGHT OF THE EMER. AN UNEVENTFUL LNDG ON RWY 24L WAS MADE. AS WE CLRED THE RWY, THE #1 ENG WAS SHUTDOWN AND A SINGLE TAXI MADE TO THE GATE. THE CAUSE OF THE ENG FAILURE WAS FOUND TO BE A BEARING FAILURE. MY THANKS TO THE CAPT FOR A JOB WELL DONE FROM THE LEFT SEAT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.