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|
Attributes | |
ACN | 161908 |
Time | |
Date | 199010 |
Day | Wed |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : tyo |
State Reference | FO |
Altitude | msl bound lower : 39300 msl bound upper : 41000 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : rjtg |
Operator | common carrier : air carrier |
Make Model Name | Widebody, Low Wing, 4 Turbojet Eng |
Navigation In Use | Other |
Flight Phase | cruise other |
Route In Use | enroute : other oceanic enroute : pacific enroute other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : second officer |
Qualification | pilot : commercial pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 250 flight time total : 5550 flight time type : 1800 |
ASRS Report | 161908 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : less severe altitude deviation : excursion from assigned altitude inflight encounter : weather other anomaly other spatial deviation |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : returned to intended course or assigned course flight crew : overcame equipment problem |
Consequence | Other |
Supplementary | |
Primary Problem | Weather |
Air Traffic Incident | other |
Narrative:
Encountered a rather strong takeoff at approximately 157 degrees east en route hnl-nrt. At FL410, moderate-heavy turbulence, static air temperature rise from -63 to -30 degrees. Engines #1, #3 and #4 compressor stalled. Aircraft descended from 41000 to 39300' and deviated approximately 7 NM right course west/O clearance. Descent required due to loss of thrust. Once clear of WX climbed back to FL410 and reported to tokyo and hnl radio. Flight continued to destination with no further problems.
Original NASA ASRS Text
Title: ACR WDB LOST 1700' AND DEVIATED 7 NM OFF TRACK WHEN 3 ENGINES HAD A COMPRESSOR STALL AS THE ACFT TRANSITED A HIGH LEVEL TKOF AT FL410.
Narrative: ENCOUNTERED A RATHER STRONG TKOF AT APPROX 157 DEGS E ENRTE HNL-NRT. AT FL410, MODERATE-HEAVY TURB, STATIC AIR TEMP RISE FROM -63 TO -30 DEGS. ENGS #1, #3 AND #4 COMPRESSOR STALLED. ACFT DSNDED FROM 41000 TO 39300' AND DEVIATED APPROX 7 NM RIGHT COURSE W/O CLRNC. DSNT REQUIRED DUE TO LOSS OF THRUST. ONCE CLR OF WX CLBED BACK TO FL410 AND RPTED TO TOKYO AND HNL RADIO. FLT CONTINUED TO DEST WITH NO FURTHER PROBS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.