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|
Attributes | |
ACN | 186916 |
Time | |
Date | 199108 |
Day | Sun |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : lex |
State Reference | KY |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Aircraft 1 | |
Operator | general aviation : personal |
Make Model Name | Small Aircraft, Low Wing, 1 Eng, Fixed Gear |
Flight Phase | landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : single pilot |
Qualification | pilot : atp pilot : flight engineer pilot : instrument pilot : commercial |
Experience | flight time last 90 days : 150 flight time total : 15000 flight time type : 4 |
ASRS Report | 186916 |
Person 2 | |
Affiliation | government : faa |
Function | controller : local |
Qualification | controller : non radar |
Events | |
Anomaly | conflict : ground less severe inflight encounter : weather other anomaly other anomaly other |
Independent Detector | other other : unspecified cockpit |
Resolutory Action | none taken : insufficient time none taken : anomaly accepted |
Consequence | other Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
Cleared to land runway 22 lex, encountered turbulence from departing turboprop. Had a hard landing resulting in a collapsed nose wheel, stopped aircraft on runway, winds were light. Viewpoints of why: first of all, as an airline pilot, flying the large transport, I was not successful in converting my habit patterns to light plane flying. The spacing behind the departing 'small' turboprop seemed ok if I had been flying the large transport but proved to be too close for the light airplane I now was in. Should have opted for greater spacing. Once in the landing turbulence, I tried to save the landing, since there was plenty of runway. I should have gone around and did not recognize the need based on my heavy jet mind frame. When in trouble my natural reactions to trying to save the landing reverted back to actions on the large transport. I believe that fatigue was a big factor in my poor performance since I had never had this problem before.
Original NASA ASRS Text
Title: SMA ACFT CAUGHT IN VORTICES FROM ACFT TAKING OFF. PLT OF SMA LOST CTL AND COLLAPSED NOSE WHEEL IN HARD LNDG.
Narrative: CLRED TO LAND RWY 22 LEX, ENCOUNTERED TURB FROM DEPARTING TURBOPROP. HAD A HARD LNDG RESULTING IN A COLLAPSED NOSE WHEEL, STOPPED ACFT ON RWY, WINDS WERE LIGHT. VIEWPOINTS OF WHY: FIRST OF ALL, AS AN AIRLINE PLT, FLYING THE LGT, I WAS NOT SUCCESSFUL IN CONVERTING MY HABIT PATTERNS TO LIGHT PLANE FLYING. THE SPACING BEHIND THE DEPARTING 'SMALL' TURBOPROP SEEMED OK IF I HAD BEEN FLYING THE LGT BUT PROVED TO BE TOO CLOSE FOR THE LIGHT AIRPLANE I NOW WAS IN. SHOULD HAVE OPTED FOR GREATER SPACING. ONCE IN THE LNDG TURB, I TRIED TO SAVE THE LNDG, SINCE THERE WAS PLENTY OF RWY. I SHOULD HAVE GONE AROUND AND DID NOT RECOGNIZE THE NEED BASED ON MY HVY JET MIND FRAME. WHEN IN TROUBLE MY NATURAL REACTIONS TO TRYING TO SAVE THE LNDG REVERTED BACK TO ACTIONS ON THE LGT. I BELIEVE THAT FATIGUE WAS A BIG FACTOR IN MY POOR PERFORMANCE SINCE I HAD NEVER HAD THIS PROBLEM BEFORE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.