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|
Attributes | |
ACN | 196103 |
Time | |
Date | 199112 |
Day | Wed |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : tul |
State Reference | OK |
Altitude | msl bound lower : 1000 msl bound upper : 1000 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tracon : tul tower : tul tower : eri |
Operator | common carrier : air carrier |
Make Model Name | Large Transport, Low Wing, 3 Turbojet Eng |
Flight Phase | climbout : takeoff landing other other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : commercial pilot : instrument |
Experience | flight time last 90 days : 75 flight time total : 20000 |
ASRS Report | 196103 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : atp pilot : instrument |
Experience | flight time total : 5500 flight time type : 200 |
ASRS Report | 195898 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : regained aircraft control other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
This is a follow up for your information, report filed on this incident 12/X/91. Large transport came out of 'C' check locking pin not removed from right ground spoilers. Ground spoilers locked in full extended position (should have had red flag attached to pin, none attached). Not detected on preflight as company procedure is to deploy all spoilers prior to outside walk around, so all spoilers were up during flight engineer check, which is normal. There is no requirement to check spoiler retraction once speed brake handle returned to stowed position. So! We took off with spoiler up. It caused roll and yaw plus caused #3 engine to violently compressor stall continuously until shut down. Roll problem quite severe. 5 units rudder 50 degree left aileron -- to fly straight -- very little ability to turn left. (Thrust from #1 plus spoiler). Landed uneventfully. Fortunately I am an large transport check captain and we experimented around with this stuff in the simulator all the time, so it wasn't a big deal, but coupled with bad WX or mexico city, etc. It could have been a disaster. Supplemental information from acn 195898. After takeoff (captain flying) aircraft flight controls had a problem and #3 engine started compressor stalling. A precautionary shutdown was accomplished and fuel was dumped. Flight controls still had a major problem. An emergency was declared and fire trucks were standing by for us. We found our inboard right ground spoilers were fully deployed. At this time maintenance thinks that a lock out was forgotten by maintenance after a heavy 'C' check, and the disrupted air after takeoff flamed-out our #3 engine, and caused the obvious flight control problems.
Original NASA ASRS Text
Title: FLC OF LGT TOOK OFF WITH R GND SPOILERS EXTENDED.
Narrative: THIS IS A FOLLOW UP FOR YOUR INFO, RPT FILED ON THIS INCIDENT 12/X/91. LGT CAME OUT OF 'C' CHK LOCKING PIN NOT REMOVED FROM R GND SPOILERS. GND SPOILERS LOCKED IN FULL EXTENDED POS (SHOULD HAVE HAD RED FLAG ATTACHED TO PIN, NONE ATTACHED). NOT DETECTED ON PREFLT AS COMPANY PROC IS TO DEPLOY ALL SPOILERS PRIOR TO OUTSIDE WALK AROUND, SO ALL SPOILERS WERE UP DURING FLT ENGINEER CHK, WHICH IS NORMAL. THERE IS NO REQUIREMENT TO CHK SPOILER RETRACTION ONCE SPD BRAKE HANDLE RETURNED TO STOWED POS. SO! WE TOOK OFF WITH SPOILER UP. IT CAUSED ROLL AND YAW PLUS CAUSED #3 ENG TO VIOLENTLY COMPRESSOR STALL CONTINUOUSLY UNTIL SHUT DOWN. ROLL PROBLEM QUITE SEVERE. 5 UNITS RUDDER 50 DEG L AILERON -- TO FLY STRAIGHT -- VERY LITTLE ABILITY TO TURN L. (THRUST FROM #1 PLUS SPOILER). LANDED UNEVENTFULLY. FORTUNATELY I AM AN LGT CHK CAPT AND WE EXPERIMENTED AROUND WITH THIS STUFF IN THE SIMULATOR ALL THE TIME, SO IT WASN'T A BIG DEAL, BUT COUPLED WITH BAD WX OR MEXICO CITY, ETC. IT COULD HAVE BEEN A DISASTER. SUPPLEMENTAL INFO FROM ACN 195898. AFTER TKOF (CAPT FLYING) ACFT FLT CTLS HAD A PROBLEM AND #3 ENG STARTED COMPRESSOR STALLING. A PRECAUTIONARY SHUTDOWN WAS ACCOMPLISHED AND FUEL WAS DUMPED. FLT CTLS STILL HAD A MAJOR PROBLEM. AN EMER WAS DECLARED AND FIRE TRUCKS WERE STANDING BY FOR US. WE FOUND OUR INBOARD R GND SPOILERS WERE FULLY DEPLOYED. AT THIS TIME MAINT THINKS THAT A LOCK OUT WAS FORGOTTEN BY MAINT AFTER A HVY 'C' CHK, AND THE DISRUPTED AIR AFTER TKOF FLAMED-OUT OUR #3 ENG, AND CAUSED THE OBVIOUS FLT CTL PROBLEMS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.