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|
Attributes | |
ACN | 208932 |
Time | |
Date | 199204 |
Day | Tue |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : apa |
State Reference | CO |
Altitude | msl bound lower : 10000 msl bound upper : 10000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | general aviation : corporate |
Make Model Name | Small Aircraft, Low Wing, 2 Eng, Retractable Gear |
Flight Phase | cruise other |
Route In Use | enroute airway : zdv |
Flight Plan | IFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : instrument pilot : commercial |
Experience | flight time total : 1900 |
ASRS Report | 208932 |
Person 2 | |
Affiliation | government : faa |
Function | controller : radar |
Qualification | controller : radar |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | none taken : unable other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
15 mins out of burlington, co, level 10000 ft, I experienced about 30 seconds of electrical failure, first recognized by the pitch of the autoplt. After disengaging the autoplt and establishing level flight, annunciator panel and radios failed for about 30 seconds, then came back on line for about 2 mins. I was able to advise denver center of the problem. They responded that they had a good primary radar target on the aircraft and to continue on, they would be able to track the aircraft to apa. I was unable to locate problem and ended up shutting down the master. After uneventful landing at apa, mechanics found a STAR washer shorted across magnetic-starter switch poles. Aircraft was 6 hours out of paint and upholstery. Washer was lost off of left generator switch behind panel, and eventually worked it's way into left magnetic-starter switch, causing starter to engage in flight resulting in electrical overload (amp meters read 35 and 40 amps). Gremlins ran wild in avionics, even causing audi through overhead speaker when audio was not in the speakers position. Without a high voltage light or panel breaker, it was impossible to find problem in flight. Thankfully it was good VFR day.
Original NASA ASRS Text
Title: PRIMARY ELECTRICAL SUPPLY PROBLEM.
Narrative: 15 MINS OUT OF BURLINGTON, CO, LEVEL 10000 FT, I EXPERIENCED ABOUT 30 SECONDS OF ELECTRICAL FAILURE, FIRST RECOGNIZED BY THE PITCH OF THE AUTOPLT. AFTER DISENGAGING THE AUTOPLT AND ESTABLISHING LEVEL FLT, ANNUNCIATOR PANEL AND RADIOS FAILED FOR ABOUT 30 SECONDS, THEN CAME BACK ON LINE FOR ABOUT 2 MINS. I WAS ABLE TO ADVISE DENVER CTR OF THE PROBLEM. THEY RESPONDED THAT THEY HAD A GOOD PRIMARY RADAR TARGET ON THE ACFT AND TO CONTINUE ON, THEY WOULD BE ABLE TO TRACK THE ACFT TO APA. I WAS UNABLE TO LOCATE PROBLEM AND ENDED UP SHUTTING DOWN THE MASTER. AFTER UNEVENTFUL LNDG AT APA, MECHS FOUND A STAR WASHER SHORTED ACROSS MAG-STARTER SWITCH POLES. ACFT WAS 6 HRS OUT OF PAINT AND UPHOLSTERY. WASHER WAS LOST OFF OF L GENERATOR SWITCH BEHIND PANEL, AND EVENTUALLY WORKED IT'S WAY INTO L MAG-STARTER SWITCH, CAUSING STARTER TO ENGAGE IN FLT RESULTING IN ELECTRICAL OVERLOAD (AMP METERS READ 35 AND 40 AMPS). GREMLINS RAN WILD IN AVIONICS, EVEN CAUSING AUDI THROUGH OVERHEAD SPEAKER WHEN AUDIO WAS NOT IN THE SPEAKERS POS. WITHOUT A HIGH VOLTAGE LIGHT OR PANEL BREAKER, IT WAS IMPOSSIBLE TO FIND PROBLEM IN FLT. THANKFULLY IT WAS GOOD VFR DAY.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.