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|
Attributes | |
ACN | 210944 |
Time | |
Date | 199205 |
Day | Fri |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : den |
State Reference | CO |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Large Transport, Low Wing, 3 Turbojet Eng |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : second officer |
Qualification | pilot : instrument pilot : commercial pilot : atp |
Experience | flight time last 90 days : 180 flight time total : 2500 flight time type : 500 |
ASRS Report | 210944 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : flight engineer pilot : cfi pilot : atp |
Experience | flight time last 90 days : 80 |
ASRS Report | 210105 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
On initial engine runup on runway 26L at den, the #2 engine on our large transport compressor stalled. The event occurred with fairly strong xwinds existing at the time (190/14) and almost immediately after brake release. The throttles were brought to idle and we taxied clear of the runway. The engine recovered to normal idle indications. An engine runup was performed and it was determined that the engine was running fine. A normal takeoff was performed and the flight continued on uneventfully. Supplemental information from acn 210105. The first officer, uncharacteristically, advanced the throttles too quickly for the conditions and the #2 engine stalled. I should have briefed proper throttle movement with a crosswind. We turned off the runway and, with tower's permission, advanced #2 engine to takeoff power. All indications were normal so I taxied back for an uneventful takeoff.
Original NASA ASRS Text
Title: LGT ABORTS TKOF AS #2 ENG COMPRESSOR STALLS.
Narrative: ON INITIAL ENG RUNUP ON RWY 26L AT DEN, THE #2 ENG ON OUR LGT COMPRESSOR STALLED. THE EVENT OCCURRED WITH FAIRLY STRONG XWINDS EXISTING AT THE TIME (190/14) AND ALMOST IMMEDIATELY AFTER BRAKE RELEASE. THE THROTTLES WERE BROUGHT TO IDLE AND WE TAXIED CLR OF THE RWY. THE ENG RECOVERED TO NORMAL IDLE INDICATIONS. AN ENG RUNUP WAS PERFORMED AND IT WAS DETERMINED THAT THE ENG WAS RUNNING FINE. A NORMAL TKOF WAS PERFORMED AND THE FLT CONTINUED ON UNEVENTFULLY. SUPPLEMENTAL INFO FROM ACN 210105. THE FO, UNCHARACTERISTICALLY, ADVANCED THE THROTTLES TOO QUICKLY FOR THE CONDITIONS AND THE #2 ENG STALLED. I SHOULD HAVE BRIEFED PROPER THROTTLE MOVEMENT WITH A XWIND. WE TURNED OFF THE RWY AND, WITH TWR'S PERMISSION, ADVANCED #2 ENG TO TKOF PWR. ALL INDICATIONS WERE NORMAL SO I TAXIED BACK FOR AN UNEVENTFUL TKOF.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.