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|
Attributes | |
ACN | 211098 |
Time | |
Date | 199205 |
Day | Mon |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : lcg |
State Reference | NE |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | general aviation : corporate |
Make Model Name | Small Transport, Low Wing, 2 Recip Eng |
Flight Phase | landing other |
Flight Plan | VFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 65 flight time total : 4050 flight time type : 900 |
ASRS Report | 211098 |
Person 2 | |
Affiliation | Other |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency none taken : insufficient time |
Consequence | other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
The flight started out of rap ending in lcg. I entered the traffic pattern and lowered the landing gear and got 3 green lights. I was landing on runway 4 at lcg with a wind at about 40 degree to the runway. Upon landing the left main touched down and the right wing went to the concrete with my right propeller also striking. I continued down the runway for some distance until I went off the runway facing south. My wife was aboard. No injuries. I do have witnesses. I called FSS and reported what had happened and they got me in contact with the FAA. Until this point the flight was uneventful, lasting 1.5 hours. I secured the aircraft prior to calling flight service. I had at least 9 hours of sleep the night before.
Original NASA ASRS Text
Title: SMT GEAR COLLAPSED AT TOUCHDOWN.
Narrative: THE FLT STARTED OUT OF RAP ENDING IN LCG. I ENTERED THE TFC PATTERN AND LOWERED THE LNDG GEAR AND GOT 3 GREEN LIGHTS. I WAS LNDG ON RWY 4 AT LCG WITH A WIND AT ABOUT 40 DEG TO THE RWY. UPON LNDG THE L MAIN TOUCHED DOWN AND THE R WING WENT TO THE CONCRETE WITH MY R PROP ALSO STRIKING. I CONTINUED DOWN THE RWY FOR SOME DISTANCE UNTIL I WENT OFF THE RWY FACING S. MY WIFE WAS ABOARD. NO INJURIES. I DO HAVE WITNESSES. I CALLED FSS AND RPTED WHAT HAD HAPPENED AND THEY GOT ME IN CONTACT WITH THE FAA. UNTIL THIS POINT THE FLT WAS UNEVENTFUL, LASTING 1.5 HRS. I SECURED THE ACFT PRIOR TO CALLING FLT SVC. I HAD AT LEAST 9 HRS OF SLEEP THE NIGHT BEFORE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.