37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 214785 |
Time | |
Date | 199207 |
Day | Tue |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : dca |
State Reference | DC |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : bdl |
Operator | common carrier : air carrier |
Make Model Name | Medium Transport, High Wing, 2 Turboprop Eng |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 120 flight time total : 7000 flight time type : 2700 |
ASRS Report | 214785 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
On takeoff roll small torque fluctuation of 2-4 percent on #2 engine look like erratic gauge. Call V1 vr (same 94 KTS) at same time torque started large fluctuation of 10-15 percent. Call for abort and to settle the aircraft back down on the runway. Normal deceleration and normal braking to full stop. Taxied off end of runway 3. Passenger complained of hard landing and back pain. Aircraft had just started rotation when call for abort was initiated. Aircraft broke ground. As PIC the safest action at that moment was to reduce power and settle and back onto the runway even after V1, vr was called.
Original NASA ASRS Text
Title: ACR MLG ACFT ABORTED TKOF DUE TO ENG MALFUNCTION.
Narrative: ON TKOF ROLL SMALL TORQUE FLUCTUATION OF 2-4 PERCENT ON #2 ENG LOOK LIKE ERRATIC GAUGE. CALL V1 VR (SAME 94 KTS) AT SAME TIME TORQUE STARTED LARGE FLUCTUATION OF 10-15 PERCENT. CALL FOR ABORT AND TO SETTLE THE ACFT BACK DOWN ON THE RWY. NORMAL DECELERATION AND NORMAL BRAKING TO FULL STOP. TAXIED OFF END OF RWY 3. PAX COMPLAINED OF HARD LNDG AND BACK PAIN. ACFT HAD JUST STARTED ROTATION WHEN CALL FOR ABORT WAS INITIATED. ACFT BROKE GND. AS PIC THE SAFEST ACTION AT THAT MOMENT WAS TO REDUCE PWR AND SETTLE AND BACK ONTO THE RWY EVEN AFTER V1, VR WAS CALLED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.