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|
Attributes | |
ACN | 230293 |
Time | |
Date | 199301 |
Day | Mon |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : chs |
State Reference | SC |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Operator | common carrier : air taxi |
Make Model Name | Light Transport, Low Wing, 2 Turboprop Eng |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air taxi |
Function | flight crew : captain oversight : pic |
Qualification | pilot : commercial pilot : cfi pilot : atp |
Experience | flight time last 90 days : 150 flight time total : 4000 flight time type : 1300 |
ASRS Report | 230293 |
Person 2 | |
Affiliation | company : air taxi |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far |
Independent Detector | other flight crewa |
Resolutory Action | none taken : anomaly accepted |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation |
Narrative:
When we attempted a takeoff from runway 21 at chs, the first officer was flying. V1 was 101 KTS. Upon reaching approximately 95 KTS, the #2 engine started to bypass fuel, resulting in a loss of between 10-15 percent torque. This caused a noticeable yaw to the right. The first officer called 'malfunction.' I called 'reject' and took command of the airplane. We instructed chs tower we wished to taxi back to conduct a run-up. During the run-up, all engine parameters were normal and the previous condition could not be reproduced. We proceeded with another takeoff and completed it successfully.
Original NASA ASRS Text
Title: LTT ABORTS TKOF WHEN AN ENG LOSES PWR.
Narrative: WHEN WE ATTEMPTED A TKOF FROM RWY 21 AT CHS, THE FO WAS FLYING. V1 WAS 101 KTS. UPON REACHING APPROX 95 KTS, THE #2 ENG STARTED TO BYPASS FUEL, RESULTING IN A LOSS OF BTWN 10-15 PERCENT TORQUE. THIS CAUSED A NOTICEABLE YAW TO THE R. THE FO CALLED 'MALFUNCTION.' I CALLED 'REJECT' AND TOOK COMMAND OF THE AIRPLANE. WE INSTRUCTED CHS TWR WE WISHED TO TAXI BACK TO CONDUCT A RUN-UP. DURING THE RUN-UP, ALL ENG PARAMETERS WERE NORMAL AND THE PREVIOUS CONDITION COULD NOT BE REPRODUCED. WE PROCEEDED WITH ANOTHER TKOF AND COMPLETED IT SUCCESSFULLY.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.