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|
Attributes | |
ACN | 230734 |
Time | |
Date | 199301 |
Day | Sat |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : mci airport : cmi |
State Reference | IL |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Dawn |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Medium Transport, High Wing, 2 Turboprop Eng |
Navigation In Use | Other |
Flight Phase | climbout : takeoff ground other : taxi |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 180 flight time total : 15000 |
ASRS Report | 230734 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other controllera |
Resolutory Action | none taken : detected after the fact other |
Consequence | other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
On departure from runway 4 at champaign, il, en route to chicago, il, the #3 main wheel departed the aircraft. The tower informed flight of this and after contacting dispatch a decision was made to land at ft wayne, in. This was accomplished without further incidence. The problem started when completing a 180 degree turn at the end of runway 4 at cmi. The nose steering annunciator light came on and the aircraft would not straighten out. Even when using opposite brakes and differential power. Maintenance was contacted through operations and a conversation through a third party with them directed us to try what we had already done. A decision to have a local FBO straighten out the nosewheel was made. The FBO truck came out to the aircraft with 2 agents and attached a tow bar and straightened out the nosewheel. The first officer got off the plane once we shutdown the #1 engine (the #2 engine was still running) to make sure they attached the tow bar correctly and that there was no damage to the nose gear. He then got back on and asked if everything was okay but I could not turn the nose steering back on until the tow bar was disconnected. He got back off and had them disconnect. One of the agents said something about a main tire or wheel in a casual manner. The first officer indicated they looked normal to him and we started #1 engine and departed. Now after the fact, I hear the agent said 'the wheel was bent inward so far it touched the strut.' since the wheel did fall off perhaps it was bent. But I know the first officer would never knowingly get on and allow the aircraft with 37 people to depart. The aircraft taxied normally. The takeoff was normal. There was no indication of a problem. So what happened? I suspect the casual attitude of the FBO agent and the fact that the #2 engine was running and the first officer had ear plugs in combined with a 15 KT wind created an extremely noisy environment to communicate in. It was also dawn, combined with the fact that we had a problem with the nose steering not a main wheel and maintenance said nothing about a main wheel we had no indication of a problem except the one comment from the FBO agent. I would like to think that any person involved in aviation would not knowingly let an aircraft depart with a problem that could cause an accident. I know those of us on the flight deck would never have allowed the aircraft to depart had we known of this problem. Perhaps the agent could have been more adamant. A direct link to maintenance could have helped. Could the aircraft manufacturer have helped troubleshoot?
Original NASA ASRS Text
Title: MDT HAS 1 MAIN GEAR TIRE DEPART THE ACFT ON TKOF. DIVERSION TO ALTERNATE ARPT.
Narrative: ON DEP FROM RWY 4 AT CHAMPAIGN, IL, ENRTE TO CHICAGO, IL, THE #3 MAIN WHEEL DEPARTED THE ACFT. THE TWR INFORMED FLT OF THIS AND AFTER CONTACTING DISPATCH A DECISION WAS MADE TO LAND AT FT WAYNE, IN. THIS WAS ACCOMPLISHED WITHOUT FURTHER INCIDENCE. THE PROB STARTED WHEN COMPLETING A 180 DEG TURN AT THE END OF RWY 4 AT CMI. THE NOSE STEERING ANNUNCIATOR LIGHT CAME ON AND THE ACFT WOULD NOT STRAIGHTEN OUT. EVEN WHEN USING OPPOSITE BRAKES AND DIFFERENTIAL PWR. MAINT WAS CONTACTED THROUGH OPS AND A CONVERSATION THROUGH A THIRD PARTY WITH THEM DIRECTED US TO TRY WHAT WE HAD ALREADY DONE. A DECISION TO HAVE A LCL FBO STRAIGHTEN OUT THE NOSEWHEEL WAS MADE. THE FBO TRUCK CAME OUT TO THE ACFT WITH 2 AGENTS AND ATTACHED A TOW BAR AND STRAIGHTENED OUT THE NOSEWHEEL. THE FO GOT OFF THE PLANE ONCE WE SHUTDOWN THE #1 ENG (THE #2 ENG WAS STILL RUNNING) TO MAKE SURE THEY ATTACHED THE TOW BAR CORRECTLY AND THAT THERE WAS NO DAMAGE TO THE NOSE GEAR. HE THEN GOT BACK ON AND ASKED IF EVERYTHING WAS OKAY BUT I COULD NOT TURN THE NOSE STEERING BACK ON UNTIL THE TOW BAR WAS DISCONNECTED. HE GOT BACK OFF AND HAD THEM DISCONNECT. ONE OF THE AGENTS SAID SOMETHING ABOUT A MAIN TIRE OR WHEEL IN A CASUAL MANNER. THE FO INDICATED THEY LOOKED NORMAL TO HIM AND WE STARTED #1 ENG AND DEPARTED. NOW AFTER THE FACT, I HEAR THE AGENT SAID 'THE WHEEL WAS BENT INWARD SO FAR IT TOUCHED THE STRUT.' SINCE THE WHEEL DID FALL OFF PERHAPS IT WAS BENT. BUT I KNOW THE FO WOULD NEVER KNOWINGLY GET ON AND ALLOW THE ACFT WITH 37 PEOPLE TO DEPART. THE ACFT TAXIED NORMALLY. THE TKOF WAS NORMAL. THERE WAS NO INDICATION OF A PROB. SO WHAT HAPPENED? I SUSPECT THE CASUAL ATTITUDE OF THE FBO AGENT AND THE FACT THAT THE #2 ENG WAS RUNNING AND THE FO HAD EAR PLUGS IN COMBINED WITH A 15 KT WIND CREATED AN EXTREMELY NOISY ENVIRONMENT TO COMMUNICATE IN. IT WAS ALSO DAWN, COMBINED WITH THE FACT THAT WE HAD A PROB WITH THE NOSE STEERING NOT A MAIN WHEEL AND MAINT SAID NOTHING ABOUT A MAIN WHEEL WE HAD NO INDICATION OF A PROB EXCEPT THE ONE COMMENT FROM THE FBO AGENT. I WOULD LIKE TO THINK THAT ANY PERSON INVOLVED IN AVIATION WOULD NOT KNOWINGLY LET AN ACFT DEPART WITH A PROB THAT COULD CAUSE AN ACCIDENT. I KNOW THOSE OF US ON THE FLT DECK WOULD NEVER HAVE ALLOWED THE ACFT TO DEPART HAD WE KNOWN OF THIS PROB. PERHAPS THE AGENT COULD HAVE BEEN MORE ADAMANT. A DIRECT LINK TO MAINT COULD HAVE HELPED. COULD THE ACFT MANUFACTURER HAVE HELPED TROUBLESHOOT?
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.