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|
Attributes | |
ACN | 234257 |
Time | |
Date | 199302 |
Day | Wed |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : i77 |
State Reference | OH |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air taxi |
Make Model Name | Small Transport, Low Wing, 2 Recip Eng |
Flight Phase | descent : approach landing other |
Flight Plan | None |
Person 1 | |
Affiliation | company : air taxi |
Function | flight crew : single pilot |
Qualification | pilot : cfi pilot : commercial pilot : instrument |
Experience | flight time last 90 days : 210 flight time total : 2100 flight time type : 285 |
ASRS Report | 234257 |
Events | |
Anomaly | other anomaly other spatial deviation |
Independent Detector | other flight crewa |
Resolutory Action | none taken : unable |
Consequence | other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
On final approach the aircraft developed a high sink rate and landed about 30 ft short of the threshold. It had snowed heavily 2 days earlier and the aircraft rolled through a 2-3 ft high snow bank at the runway threshold which sheared a bolt in the left main gear. At about 900 ft down the runway the bolt fell out of the gear causing the aircraft to settle on the left engine nacelle. The aircraft came to rest on a snow bank on the left side of the runway with damage to the propeller and flap on the left side in addition to the sheared bolt. The local authorities and the FAA GADO inspector responded and documented the incident. This runway is closely bounded on both sides by woods. At the time of the incident the wind was about 10-13 KTS at 45 degrees across the runway. As the aircraft descended below 200 ft AGL the wind sheared off rapidly behind the trees. This led to a rapid decrease in airspeed and rapid increase in sink rate which I did not fully perceive until the aircraft had gotten 'behind the power curve.' I was aware of an increase in sink rate but I did not add sufficient power to overcome it as, for the reasons stated above, I did not properly judge how excessive it had become until it was too late to recover.
Original NASA ASRS Text
Title: SMT UNDERSHOOTS RWY, PLOWS THROUGH SNOW BANK AND L MAIN GEAR COLLAPSES DURING LNDG ROLLOUT.
Narrative: ON FINAL APCH THE ACFT DEVELOPED A HIGH SINK RATE AND LANDED ABOUT 30 FT SHORT OF THE THRESHOLD. IT HAD SNOWED HEAVILY 2 DAYS EARLIER AND THE ACFT ROLLED THROUGH A 2-3 FT HIGH SNOW BANK AT THE RWY THRESHOLD WHICH SHEARED A BOLT IN THE L MAIN GEAR. AT ABOUT 900 FT DOWN THE RWY THE BOLT FELL OUT OF THE GEAR CAUSING THE ACFT TO SETTLE ON THE L ENG NACELLE. THE ACFT CAME TO REST ON A SNOW BANK ON THE L SIDE OF THE RWY WITH DAMAGE TO THE PROP AND FLAP ON THE L SIDE IN ADDITION TO THE SHEARED BOLT. THE LCL AUTHORITIES AND THE FAA GADO INSPECTOR RESPONDED AND DOCUMENTED THE INCIDENT. THIS RWY IS CLOSELY BOUNDED ON BOTH SIDES BY WOODS. AT THE TIME OF THE INCIDENT THE WIND WAS ABOUT 10-13 KTS AT 45 DEGS ACROSS THE RWY. AS THE ACFT DSNDED BELOW 200 FT AGL THE WIND SHEARED OFF RAPIDLY BEHIND THE TREES. THIS LED TO A RAPID DECREASE IN AIRSPD AND RAPID INCREASE IN SINK RATE WHICH I DID NOT FULLY PERCEIVE UNTIL THE ACFT HAD GOTTEN 'BEHIND THE PWR CURVE.' I WAS AWARE OF AN INCREASE IN SINK RATE BUT I DID NOT ADD SUFFICIENT PWR TO OVERCOME IT AS, FOR THE REASONS STATED ABOVE, I DID NOT PROPERLY JUDGE HOW EXCESSIVE IT HAD BECOME UNTIL IT WAS TOO LATE TO RECOVER.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.