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|
Attributes | |
ACN | 242088 |
Time | |
Date | 199305 |
Day | Wed |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : gcn |
State Reference | AZ |
Altitude | agl bound lower : 0 agl bound upper : 200 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : gcn |
Operator | common carrier : air carrier |
Make Model Name | Small Transport |
Flight Phase | climbout : takeoff climbout : initial ground : holding |
Flight Plan | None |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial pilot : atp |
Experience | flight time last 90 days : 250 flight time total : 3000 flight time type : 2000 |
ASRS Report | 242088 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far other anomaly other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : overcame equipment problem flight crew : regained aircraft control |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Right after V1 call aircraft made sharp roll to the left, initial thought was an engine failure. After checking gauges and finding nothing wrong, I looked down to my left and noticed aileron trim was showing a full deflection to the left. The captain also noticed the same. I helped with the controls to level aircraft after which the captain gave over controls to me while he ran the trim back and pulled the circuit breaker. The runway is cut out amongst the trees so after getting everything situated we cleared the trees by about 100-200 ft. The flight continued without further incident. Initial assessment was a runaway trim tab, but it probably would not have returned to center. The next day I remembered that a passenger poked into the cockpit while we were at the hold line inquiring about her head seat. Trim tab is located right at the entrance to cockpit, passenger probably leaned on trim tab actuator (which is a rocker switch) and ran it all the way to left. Situation could have been avoided by either having a cockpit door or by putting a guard over the switch.
Original NASA ASRS Text
Title: FLC OF AN ACR SMT TWIN ENG TURBO PROP ACFT MOMENTARILY LOST CTL OF THE ACFT ON TKOF DUE TO THE AILERON TRIM TAB SET ALL THE WAY TO THE L.
Narrative: RIGHT AFTER V1 CALL ACFT MADE SHARP ROLL TO THE L, INITIAL THOUGHT WAS AN ENG FAILURE. AFTER CHKING GAUGES AND FINDING NOTHING WRONG, I LOOKED DOWN TO MY L AND NOTICED AILERON TRIM WAS SHOWING A FULL DEFLECTION TO THE L. THE CAPT ALSO NOTICED THE SAME. I HELPED WITH THE CTLS TO LEVEL ACFT AFTER WHICH THE CAPT GAVE OVER CTLS TO ME WHILE HE RAN THE TRIM BACK AND PULLED THE CIRCUIT BREAKER. THE RWY IS CUT OUT AMONGST THE TREES SO AFTER GETTING EVERYTHING SITUATED WE CLRED THE TREES BY ABOUT 100-200 FT. THE FLT CONTINUED WITHOUT FURTHER INCIDENT. INITIAL ASSESSMENT WAS A RUNAWAY TRIM TAB, BUT IT PROBABLY WOULD NOT HAVE RETURNED TO CENTER. THE NEXT DAY I REMEMBERED THAT A PAX POKED INTO THE COCKPIT WHILE WE WERE AT THE HOLD LINE INQUIRING ABOUT HER HEAD SEAT. TRIM TAB IS LOCATED RIGHT AT THE ENTRANCE TO COCKPIT, PAX PROBABLY LEANED ON TRIM TAB ACTUATOR (WHICH IS A ROCKER SWITCH) AND RAN IT ALL THE WAY TO L. SIT COULD HAVE BEEN AVOIDED BY EITHER HAVING A COCKPIT DOOR OR BY PUTTING A GUARD OVER THE SWITCH.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.