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|
Attributes | |
ACN | 244415 |
Time | |
Date | 199306 |
Day | Sun |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : hya |
State Reference | MA |
Altitude | agl bound lower : 600 agl bound upper : 600 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : hya |
Operator | general aviation : personal |
Make Model Name | Small Aircraft |
Flight Phase | climbout : takeoff landing other other |
Flight Plan | None |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : private |
Experience | flight time last 90 days : 30 flight time total : 2400 |
ASRS Report | 244415 |
Person 2 | |
Affiliation | government : faa |
Function | controller : local |
Qualification | controller : non radar |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
I was cleared for takeoff on runway 6, to make left traffic for takeoff and landing practice. At approximately 600 ft above the ground, the engine stopped. I returned to the airport and landed on runway 24, after declaring an emergency. I went off the runway on to the grass on the rollout, and stopped. There were no injuries or damage to the aircraft or anything on the ground. Subsequent investigation revealed that the friction lock on the mixture control was not properly engaged. Allowing the mixture control to vibrate out to idle cutoff. A practiced emergency cockpit checklist would have revealed the mixture control in the wrong position. I could have adjusted it properly and the engine would have restarted.
Original NASA ASRS Text
Title: BIPLANE HAS ENG FAILURE ON TKOF. ABLE TO TURN BACK TO ARPT FOR LNDG.
Narrative: I WAS CLRED FOR TKOF ON RWY 6, TO MAKE L TFC FOR TKOF AND LNDG PRACTICE. AT APPROX 600 FT ABOVE THE GND, THE ENG STOPPED. I RETURNED TO THE ARPT AND LANDED ON RWY 24, AFTER DECLARING AN EMER. I WENT OFF THE RWY ON TO THE GRASS ON THE ROLLOUT, AND STOPPED. THERE WERE NO INJURIES OR DAMAGE TO THE ACFT OR ANYTHING ON THE GND. SUBSEQUENT INVESTIGATION REVEALED THAT THE FRICTION LOCK ON THE MIXTURE CTL WAS NOT PROPERLY ENGAGED. ALLOWING THE MIXTURE CTL TO VIBRATE OUT TO IDLE CUTOFF. A PRACTICED EMER COCKPIT CHKLIST WOULD HAVE REVEALED THE MIXTURE CTL IN THE WRONG POS. I COULD HAVE ADJUSTED IT PROPERLY AND THE ENG WOULD HAVE RESTARTED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.