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|
Attributes | |
ACN | 265772 |
Time | |
Date | 199403 |
Day | Wed |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : roa |
State Reference | VA |
Altitude | msl bound lower : 6000 msl bound upper : 6000 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air taxi |
Make Model Name | Baron 58/58TC |
Operating Under FAR Part | Part 135 |
Flight Phase | cruise other |
Route In Use | enroute airway : roa |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air taxi |
Function | flight crew : single pilot |
Qualification | pilot : cfi pilot : atp |
Experience | flight time last 90 days : 40 flight time total : 2800 flight time type : 100 |
ASRS Report | 265772 |
Person 2 | |
Affiliation | government : faa |
Function | controller : approach |
Qualification | controller : radar |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | controller : issued new clearance other |
Consequence | Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
On the morning of mar/wed/94, I was acting as PIC for a single pilot flight in a beechcraft baron (BE58) that was on a charter flight from raleigh, nc, to charleston, wv. In preparation for this flight, the calculations for aircraft weight and balance indicated that a maximum fuel load could not be greater than approximately 90 gallons. The procedure used for fuel load computation on this aircraft (1973 BE58) is to record the gallons loaded in a daily aircraft log and compare fuel load to hours flown to determine fuel remaining at the end of each flight. The aircraft fuel gauges are not presently used as an accurate indicator of actual fuel load. Based on this data, I determined that the aircraft had approximately 90 gallons of fuel on board. The passenger were loaded and the flight departed rdu at approximately XA30. This flight was forecasted to be flown mostly IMC. While in IMC at 6000 ft MSL, approximately 45 mins into the flight, the left engine began to sputter/surge and the fuel pressure gauge began to fluctuate. Following checklist procedures, I turned on the fuel boost pump but the problem did not correct itself. I did not suspect fuel starvation but did not leave out this possibility. I suspected blockage or contamination. I immediately requested ATC assistance for vectors to the nearest airport (roa) which was approximately 20 NM to the east of my position. ATC cleared me to descend to 4000 ft MSL. While on my assigned heading and descending to 4000 ft, the left engine quit running. I determined that the best reaction would be to conserve fuel if this was, in fact, the problem. I feathered the left engine to obtain best performance and to conserve fuel. I was IMC with moderate to severe turbulence conditions. I extended the landing gear to assist in stabilizing the aircraft while continuing to attempt to maintain assigned ATC headings and altitudes. I discovered that I was not able to maintain 4000 ft MSL and keep the aircraft at or above VMC due to the turbulence. I informed ATC that I would need to continue descending. ATC vectored me away from mountainous obstructions and I continued to descend to approximately 3000 ft MSL. ATC then vectored me towards the roanoke airport. I was now out of the turbulent conditions. I raised the landing gear and maintained approximately 2700 ft MSL until visual contact was made with roanoke airport. I was cleared for an immediate visual approach to runway 33 and landed without further incident. I followed our operation specifications procedures and contacted our director of maintenance to report the problem. He stated that I should check for any fuel contaminants, check for any loose components that may be visible through engine cowling openings, and try to determine if fuel starvation may have occurred to the left engine. I had no way to determine the exact contents of the fuel tanks. There is no visual way to inspect the fuel load of this model of beech baron except when fuel is full. I drained some remaining fuel out of the left wing fuel sumps and did not see any contamination. I visually inspected the engine components through the cowling openings. No visual indication of a problem was apparent to me. I suspected fuel starvation had occurred. I loaded additional fuel into both aircraft wing tanks. I drained the fuel sumps to test for contaminants, only a small amount of water was found. I started the right engine. It operated normally. I started the left engine. It also appeared to operate normally. I performed a lengthy warm- up and then followed checklist procedures for checking the operation of a test flight within the roanoke airport area. No problems were found. I landed and performed another thorough operation check on the engines -- no problem was found. I visually inspected the engine and fuel one more time -- no problems were apparent. I determined that fuel starvation was the most probable cause. I decided that the flight could continue to our schedule destination. We departed roanoke and flew to charleston, wv, without further incident. Fuel starvation to left engine. Pilot judgement that recorded fuel load additions as compared to recorded fuel consumption were providing accurate remaining fuel balance. Inaccurate fuel quantity gauge readings. No method to visually inspect fuel quantity in tanks on this yr of beech baron.
Original NASA ASRS Text
Title: PLT OF AN SMT ATX ACFT HAD AN ENG QUIT DURING ENRTE CRUISE DUE TO FUEL STARVATION.
Narrative: ON THE MORNING OF MAR/WED/94, I WAS ACTING AS PIC FOR A SINGLE PLT FLT IN A BEECHCRAFT BARON (BE58) THAT WAS ON A CHARTER FLT FROM RALEIGH, NC, TO CHARLESTON, WV. IN PREPARATION FOR THIS FLT, THE CALCULATIONS FOR ACFT WT AND BAL INDICATED THAT A MAX FUEL LOAD COULD NOT BE GREATER THAN APPROX 90 GALLONS. THE PROC USED FOR FUEL LOAD COMPUTATION ON THIS ACFT (1973 BE58) IS TO RECORD THE GALLONS LOADED IN A DAILY ACFT LOG AND COMPARE FUEL LOAD TO HRS FLOWN TO DETERMINE FUEL REMAINING AT THE END OF EACH FLT. THE ACFT FUEL GAUGES ARE NOT PRESENTLY USED AS AN ACCURATE INDICATOR OF ACTUAL FUEL LOAD. BASED ON THIS DATA, I DETERMINED THAT THE ACFT HAD APPROX 90 GALLONS OF FUEL ON BOARD. THE PAX WERE LOADED AND THE FLT DEPARTED RDU AT APPROX XA30. THIS FLT WAS FORECASTED TO BE FLOWN MOSTLY IMC. WHILE IN IMC AT 6000 FT MSL, APPROX 45 MINS INTO THE FLT, THE L ENG BEGAN TO SPUTTER/SURGE AND THE FUEL PRESSURE GAUGE BEGAN TO FLUCTUATE. FOLLOWING CHKLIST PROCS, I TURNED ON THE FUEL BOOST PUMP BUT THE PROB DID NOT CORRECT ITSELF. I DID NOT SUSPECT FUEL STARVATION BUT DID NOT LEAVE OUT THIS POSSIBILITY. I SUSPECTED BLOCKAGE OR CONTAMINATION. I IMMEDIATELY REQUESTED ATC ASSISTANCE FOR VECTORS TO THE NEAREST ARPT (ROA) WHICH WAS APPROX 20 NM TO THE E OF MY POS. ATC CLRED ME TO DSND TO 4000 FT MSL. WHILE ON MY ASSIGNED HDG AND DSNDING TO 4000 FT, THE L ENG QUIT RUNNING. I DETERMINED THAT THE BEST REACTION WOULD BE TO CONSERVE FUEL IF THIS WAS, IN FACT, THE PROB. I FEATHERED THE L ENG TO OBTAIN BEST PERFORMANCE AND TO CONSERVE FUEL. I WAS IMC WITH MODERATE TO SEVERE TURB CONDITIONS. I EXTENDED THE LNDG GEAR TO ASSIST IN STABILIZING THE ACFT WHILE CONTINUING TO ATTEMPT TO MAINTAIN ASSIGNED ATC HDGS AND ALTS. I DISCOVERED THAT I WAS NOT ABLE TO MAINTAIN 4000 FT MSL AND KEEP THE ACFT AT OR ABOVE VMC DUE TO THE TURB. I INFORMED ATC THAT I WOULD NEED TO CONTINUE DSNDING. ATC VECTORED ME AWAY FROM MOUNTAINOUS OBSTRUCTIONS AND I CONTINUED TO DSND TO APPROX 3000 FT MSL. ATC THEN VECTORED ME TOWARDS THE ROANOKE ARPT. I WAS NOW OUT OF THE TURBULENT CONDITIONS. I RAISED THE LNDG GEAR AND MAINTAINED APPROX 2700 FT MSL UNTIL VISUAL CONTACT WAS MADE WITH ROANOKE ARPT. I WAS CLRED FOR AN IMMEDIATE VISUAL APCH TO RWY 33 AND LANDED WITHOUT FURTHER INCIDENT. I FOLLOWED OUR OP SPECS PROCS AND CONTACTED OUR DIRECTOR OF MAINT TO RPT THE PROB. HE STATED THAT I SHOULD CHK FOR ANY FUEL CONTAMINANTS, CHK FOR ANY LOOSE COMPONENTS THAT MAY BE VISIBLE THROUGH ENG COWLING OPENINGS, AND TRY TO DETERMINE IF FUEL STARVATION MAY HAVE OCCURRED TO THE L ENG. I HAD NO WAY TO DETERMINE THE EXACT CONTENTS OF THE FUEL TANKS. THERE IS NO VISUAL WAY TO INSPECT THE FUEL LOAD OF THIS MODEL OF BEECH BARON EXCEPT WHEN FUEL IS FULL. I DRAINED SOME REMAINING FUEL OUT OF THE L WING FUEL SUMPS AND DID NOT SEE ANY CONTAMINATION. I VISUALLY INSPECTED THE ENG COMPONENTS THROUGH THE COWLING OPENINGS. NO VISUAL INDICATION OF A PROB WAS APPARENT TO ME. I SUSPECTED FUEL STARVATION HAD OCCURRED. I LOADED ADDITIONAL FUEL INTO BOTH ACFT WING TANKS. I DRAINED THE FUEL SUMPS TO TEST FOR CONTAMINANTS, ONLY A SMALL AMOUNT OF WATER WAS FOUND. I STARTED THE R ENG. IT OPERATED NORMALLY. I STARTED THE L ENG. IT ALSO APPEARED TO OPERATE NORMALLY. I PERFORMED A LENGTHY WARM- UP AND THEN FOLLOWED CHKLIST PROCS FOR CHKING THE OP OF A TEST FLT WITHIN THE ROANOKE ARPT AREA. NO PROBS WERE FOUND. I LANDED AND PERFORMED ANOTHER THOROUGH OP CHK ON THE ENGS -- NO PROB WAS FOUND. I VISUALLY INSPECTED THE ENG AND FUEL ONE MORE TIME -- NO PROBS WERE APPARENT. I DETERMINED THAT FUEL STARVATION WAS THE MOST PROBABLE CAUSE. I DECIDED THAT THE FLT COULD CONTINUE TO OUR SCHEDULE DEST. WE DEPARTED ROANOKE AND FLEW TO CHARLESTON, WV, WITHOUT FURTHER INCIDENT. FUEL STARVATION TO L ENG. PLT JUDGEMENT THAT RECORDED FUEL LOAD ADDITIONS AS COMPARED TO RECORDED FUEL CONSUMPTION WERE PROVIDING ACCURATE REMAINING FUEL BAL. INACCURATE FUEL QUANTITY GAUGE READINGS. NO METHOD TO VISUALLY INSPECT FUEL QUANTITY IN TANKS ON THIS YR OF BEECH BARON.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.