37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 265854 |
Time | |
Date | 199403 |
Day | Fri |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : mkc |
State Reference | MO |
Altitude | msl bound lower : 2000 msl bound upper : 2000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : mkc |
Operator | general aviation : instructional |
Make Model Name | Any Unknown or Unlisted Aircraft Manufacturer |
Operating Under FAR Part | Part 91 |
Flight Phase | descent other other |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : single pilot |
Qualification | pilot : private |
Experience | flight time last 90 days : 19 flight time total : 88 flight time type : 29 |
ASRS Report | 265854 |
Person 2 | |
Affiliation | government : faa |
Function | controller : local |
Qualification | controller : non radar |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency other |
Consequence | faa : investigated |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation |
Narrative:
Earlier in the day, I had topped off both tanks and then flew for 2.2 hours, leaving me with the tanks half full. I did a flight plan from mkc to 5c8 (coffey county kansas) to do a touch-and-go at 5c8 then directly back to mkc. The distance between mkc to 5c8 is 74 NM. The winds were directly from the south at 9-15 KTS at the surface and 27 KTS above 6000 ft. I had planned the trip out to take 1:45 long. After flying for 2.2 hours earlier, I assumed that the plane would be fine for a 1 hour and 40 min trip with half tanks. I failed to do my math. Not realizing that the plane only had around 11.25 gallons and it burns around 6 per hour. The trip went fine until I was about 5 or 6 mi inbound for mkc. I was cleared to enter into a mid downwind. Pattern altitude is 1800 ft MSL and I was descending at 2000 ft when I hit some turbulence and the engine cut out. I pushed the throttle back in and the engine started back up, then hit some more and then the engine went out for good. I then set up for an engine out emergency landing. I told the controller my situation and then landed in a clear field with little problems and with very little damage to the plane.
Original NASA ASRS Text
Title: PLT OF AN SMA SEL TRAINING ACFT RAN OUT OF FUEL AND WAS FORCED TO LAND SHORT OF THE ARPT RESULTING IN VERY LITTLE DAMAGE TO THE ACFT.
Narrative: EARLIER IN THE DAY, I HAD TOPPED OFF BOTH TANKS AND THEN FLEW FOR 2.2 HRS, LEAVING ME WITH THE TANKS HALF FULL. I DID A FLT PLAN FROM MKC TO 5C8 (COFFEY COUNTY KANSAS) TO DO A TOUCH-AND-GO AT 5C8 THEN DIRECTLY BACK TO MKC. THE DISTANCE BTWN MKC TO 5C8 IS 74 NM. THE WINDS WERE DIRECTLY FROM THE S AT 9-15 KTS AT THE SURFACE AND 27 KTS ABOVE 6000 FT. I HAD PLANNED THE TRIP OUT TO TAKE 1:45 LONG. AFTER FLYING FOR 2.2 HRS EARLIER, I ASSUMED THAT THE PLANE WOULD BE FINE FOR A 1 HR AND 40 MIN TRIP WITH HALF TANKS. I FAILED TO DO MY MATH. NOT REALIZING THAT THE PLANE ONLY HAD AROUND 11.25 GALLONS AND IT BURNS AROUND 6 PER HR. THE TRIP WENT FINE UNTIL I WAS ABOUT 5 OR 6 MI INBOUND FOR MKC. I WAS CLRED TO ENTER INTO A MID DOWNWIND. PATTERN ALT IS 1800 FT MSL AND I WAS DSNDING AT 2000 FT WHEN I HIT SOME TURB AND THE ENG CUT OUT. I PUSHED THE THROTTLE BACK IN AND THE ENG STARTED BACK UP, THEN HIT SOME MORE AND THEN THE ENG WENT OUT FOR GOOD. I THEN SET UP FOR AN ENG OUT EMER LNDG. I TOLD THE CTLR MY SIT AND THEN LANDED IN A CLR FIELD WITH LITTLE PROBS AND WITH VERY LITTLE DAMAGE TO THE PLANE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.