37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 266057 |
Time | |
Date | 199403 |
Day | Sun |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : slc |
State Reference | UT |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zdv |
Operator | common carrier : air carrier |
Make Model Name | L-1011-500 Series |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | ground other : taxi |
Flight Plan | IFR |
Aircraft 2 | |
Operator | common carrier : air carrier |
Make Model Name | Commercial Fixed Wing |
Operating Under FAR Part | other : unknown |
Flight Phase | ground : parked |
Flight Plan | None |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : second officer |
Qualification | pilot : atp pilot : flight engineer pilot : commercial |
Experience | flight time total : 2500 |
ASRS Report | 266057 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | conflict : ground critical non adherence other other anomaly other |
Independent Detector | other other : unspecified |
Resolutory Action | none taken : detected after the fact |
Consequence | other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
We were delayed for maintenance from XA20 to XB14 for pushback from gate at slc. #1 and #2 engines were started and a normal pushback and taxi occurred to spot 1. We made a normal left turn from spot 1 onto taxiway H. This turn appeared very usual and did not seem to be made at excess thrust. I was busy with my station duties during the turn and did not notice the throttle position. After the turn we heard on the radio from ground and tower that a gpu unit had been blown into a commuter aircraft on the ramp and had damaged the aircraft. Thrust was used mainly on #2 engine (high, center- mounted) during turn.
Original NASA ASRS Text
Title: PARKED COMMUTER ACFT DAMAGED BY JET BLAST ENCOUNTER FROM DEP TFC IN RAMP OP ACFT DEP PROC.
Narrative: WE WERE DELAYED FOR MAINT FROM XA20 TO XB14 FOR PUSHBACK FROM GATE AT SLC. #1 AND #2 ENGS WERE STARTED AND A NORMAL PUSHBACK AND TAXI OCCURRED TO SPOT 1. WE MADE A NORMAL L TURN FROM SPOT 1 ONTO TXWY H. THIS TURN APPEARED VERY USUAL AND DID NOT SEEM TO BE MADE AT EXCESS THRUST. I WAS BUSY WITH MY STATION DUTIES DURING THE TURN AND DID NOT NOTICE THE THROTTLE POS. AFTER THE TURN WE HEARD ON THE RADIO FROM GND AND TWR THAT A GPU UNIT HAD BEEN BLOWN INTO A COMMUTER ACFT ON THE RAMP AND HAD DAMAGED THE ACFT. THRUST WAS USED MAINLY ON #2 ENG (HIGH, CTR- MOUNTED) DURING TURN.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.