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|
Attributes | |
ACN | 272050 |
Time | |
Date | 199405 |
Day | Wed |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : btv |
State Reference | VT |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | Mixed |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | SF 340A |
Operating Under FAR Part | Part 135 |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 240 flight time total : 5700 flight time type : 2000 |
ASRS Report | 272050 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far non adherence other other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : rejected takeoff flight crew : declared emergency other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation |
Narrative:
During takeoff with first officer at the controls, we aborted due to nose vibration. We taxied back to gate to inspect problem. During taxi I noticed nothing wrong and everything seemed normal. Upon reaching the gate I shut down the left engine and went outside to inspect nose gear. I noticed nothing wrong, not even a flat tire. I have over 2000 hours in this aircraft and I've experienced this before as simply a slightly loose shimmy damper that occurs on a lot of aircraft that have many hours of usage. We discussed the problem and the first officer and myself decided that it was safe to continue and we took off without further incident. Upon reaching our destination, maintenance met the aircraft. They confirmed that there was nothing wrong. They did change nosewheel tires though to possibly correct a bad tire with inner separation. I did not write up the abort in the maintenance logbook nor talk with maintenance prior to takeoff because I've had several similar occurrences before and felt that it did not warrant further investigation. I asked the mechanic if he wanted me to write it up and he replied it didn't matter, it was something simple and not to worry about it so I didn't.
Original NASA ASRS Text
Title: TKOF ABORTED DUE TO ACFT EQUIP PROB MALFUNCTION.
Narrative: DURING TKOF WITH FO AT THE CTLS, WE ABORTED DUE TO NOSE VIBRATION. WE TAXIED BACK TO GATE TO INSPECT PROB. DURING TAXI I NOTICED NOTHING WRONG AND EVERYTHING SEEMED NORMAL. UPON REACHING THE GATE I SHUT DOWN THE L ENG AND WENT OUTSIDE TO INSPECT NOSE GEAR. I NOTICED NOTHING WRONG, NOT EVEN A FLAT TIRE. I HAVE OVER 2000 HRS IN THIS ACFT AND I'VE EXPERIENCED THIS BEFORE AS SIMPLY A SLIGHTLY LOOSE SHIMMY DAMPER THAT OCCURS ON A LOT OF ACFT THAT HAVE MANY HRS OF USAGE. WE DISCUSSED THE PROB AND THE FO AND MYSELF DECIDED THAT IT WAS SAFE TO CONTINUE AND WE TOOK OFF WITHOUT FURTHER INCIDENT. UPON REACHING OUR DEST, MAINT MET THE ACFT. THEY CONFIRMED THAT THERE WAS NOTHING WRONG. THEY DID CHANGE NOSEWHEEL TIRES THOUGH TO POSSIBLY CORRECT A BAD TIRE WITH INNER SEPARATION. I DID NOT WRITE UP THE ABORT IN THE MAINT LOGBOOK NOR TALK WITH MAINT PRIOR TO TKOF BECAUSE I'VE HAD SEVERAL SIMILAR OCCURRENCES BEFORE AND FELT THAT IT DID NOT WARRANT FURTHER INVESTIGATION. I ASKED THE MECH IF HE WANTED ME TO WRITE IT UP AND HE REPLIED IT DIDN'T MATTER, IT WAS SOMETHING SIMPLE AND NOT TO WORRY ABOUT IT SO I DIDN'T.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.