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|
Attributes | |
ACN | 277851 |
Time | |
Date | 199407 |
Day | Fri |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : day |
State Reference | OH |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : lax |
Operator | common carrier : air carrier |
Make Model Name | BAe 125 Series 1000 |
Operating Under FAR Part | Part 135 |
Flight Phase | ground other : taxi |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 300 flight time total : 7000 flight time type : 300 |
ASRS Report | 277851 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
The dayton air and trade show activities changed the normal taxi route from the terminal to runway 24L. Thunderstorms/showers had been crossing the airport. We were directed to taxi from the terminal via B and F to runway 24L. Just after crossing runway 26/18 we taxied into standing water that was deeper than first appearance. As the nose tires (bae 3100) hit the water it splashed up a surprisingly large amount. This, combined with propeller interaction sent enough spray through the left engine turbine intake to cause the engine to start shutting down. In order to prevent a potentially fuel risk re-establishment of ignition, I elected to completely shutdown the engine as a normal shutdown by selecting 'stop' and then retarding the power lever to the reverse 'position.' a momentary vapor (steam?) exhaust was noted and mentioned by day ground control on 121.9. We advised that we were aware of it. Subsequently, we pulled into the runway 24L runup area and performed a restart. This restart and subsequent engine runup to power were normal. Since the shutdown was completed normally and subsequent restart and power were normal, we continued our scheduled flight.
Original NASA ASRS Text
Title: TAXIING THROUGH STANDING WATER ENG INGESTS ENOUGH WATER TO START ENG SHUT DOWN.
Narrative: THE DAYTON AIR AND TRADE SHOW ACTIVITIES CHANGED THE NORMAL TAXI RTE FROM THE TERMINAL TO RWY 24L. TSTMS/SHOWERS HAD BEEN XING THE ARPT. WE WERE DIRECTED TO TAXI FROM THE TERMINAL VIA B AND F TO RWY 24L. JUST AFTER XING RWY 26/18 WE TAXIED INTO STANDING WATER THAT WAS DEEPER THAN FIRST APPEARANCE. AS THE NOSE TIRES (BAE 3100) HIT THE WATER IT SPLASHED UP A SURPRISINGLY LARGE AMOUNT. THIS, COMBINED WITH PROP INTERACTION SENT ENOUGH SPRAY THROUGH THE L ENG TURBINE INTAKE TO CAUSE THE ENG TO START SHUTTING DOWN. IN ORDER TO PREVENT A POTENTIALLY FUEL RISK RE-ESTABLISHMENT OF IGNITION, I ELECTED TO COMPLETELY SHUTDOWN THE ENG AS A NORMAL SHUTDOWN BY SELECTING 'STOP' AND THEN RETARDING THE PWR LEVER TO THE REVERSE 'POS.' A MOMENTARY VAPOR (STEAM?) EXHAUST WAS NOTED AND MENTIONED BY DAY GND CTL ON 121.9. WE ADVISED THAT WE WERE AWARE OF IT. SUBSEQUENTLY, WE PULLED INTO THE RWY 24L RUNUP AREA AND PERFORMED A RESTART. THIS RESTART AND SUBSEQUENT ENG RUNUP TO PWR WERE NORMAL. SINCE THE SHUTDOWN WAS COMPLETED NORMALLY AND SUBSEQUENT RESTART AND PWR WERE NORMAL, WE CONTINUED OUR SCHEDULED FLT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.