37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 306012 |
Time | |
Date | 199505 |
Day | Mon |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : ord |
State Reference | IL |
Altitude | msl bound lower : 9000 msl bound upper : 9000 |
Environment | |
Flight Conditions | Mixed |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : ord |
Operator | common carrier : air carrier |
Make Model Name | MD-80 Super 80 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other |
Flight Phase | cruise other descent : approach |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 306012 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 210 flight time total : 5500 flight time type : 3500 |
ASRS Report | 306011 |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : published procedure other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency none taken : unable |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation |
Narrative:
On leveloff at 9000 ft, the #1 engine would not go above 50 percent N2. Throttle movement had no effect. Declared an emergency and requested a delaying vector. Shut down #1 engine and attempted a normal restart. On the restart the N2 would not go above 40 percent N2. Secured the #1 engine and executed a single engine approach to runway 27L. Normal approach and landing. Single engine taxi to gate. After gate arrival the fueler informed me that I had let the main tanks get out of balance. Landing weight 108000 pounds. The engine was shut down a total of 13 mins.
Original NASA ASRS Text
Title: INFLT ENG SHUTDOWN AFTER ATTEMPT IN AIR STARTING SLUGGISH ENG.
Narrative: ON LEVELOFF AT 9000 FT, THE #1 ENG WOULD NOT GO ABOVE 50 PERCENT N2. THROTTLE MOVEMENT HAD NO EFFECT. DECLARED AN EMER AND REQUESTED A DELAYING VECTOR. SHUT DOWN #1 ENG AND ATTEMPTED A NORMAL RESTART. ON THE RESTART THE N2 WOULD NOT GO ABOVE 40 PERCENT N2. SECURED THE #1 ENG AND EXECUTED A SINGLE ENG APCH TO RWY 27L. NORMAL APCH AND LNDG. SINGLE ENG TAXI TO GATE. AFTER GATE ARR THE FUELER INFORMED ME THAT I HAD LET THE MAIN TANKS GET OUT OF BAL. LNDG WT 108000 LBS. THE ENG WAS SHUT DOWN A TOTAL OF 13 MINS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.