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|
Attributes | |
ACN | 316161 |
Time | |
Date | 199509 |
Day | Tue |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : fyv |
State Reference | AR |
Altitude | msl bound lower : 13000 msl bound upper : 13000 |
Environment | |
Flight Conditions | IMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | artcc : mem |
Operator | common carrier : air carrier |
Make Model Name | SF 340A |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other |
Flight Phase | climbout : intermediate altitude landing other other |
Route In Use | enroute other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : instrument |
Experience | flight time last 90 days : 210 flight time total : 12000 flight time type : 5800 |
ASRS Report | 316161 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : unspecified |
Resolutory Action | controller : issued new clearance flight crew : overcame equipment problem other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Climbing out of 13000 ft, approximately 40 NM nnw of fsm, the cargo smoke warning illuminated on central warning panel. Bottle #1 for cargo compartment was activated and associated checklist performed. After approximately 30 seconds, the central warning panel light went out. Fsm had better WX and a longer runway, and this would be a straight line descent for us instead of fyv, right below us (a spiral descent). 12 mins later we landed without incident in FMS. #2 bottle was not used. No emergency declared. Maintenance inspected aircraft and we ferried it to dfw later. Great crew coordination. Callback conversation with reporter revealed the following information: a malfunctioning detector in the cargo compartment caused a false alarm. The photoelectric cell in the SF340 cargo compartment will detect smoke, aerosol, thick fumes, and even high humidity. Reporter states that 'when the particle interruption dissipates, then the alarms will go out.' the warning is, itself, associated with a memory checklist item for which the flight crew followed all procedures. Shortly after the flight crew had fired the bottle and had begun the 30 second timing, the flight attendant called and stated that he heard a weird noise in the cargo compartment. In fact he described the sound as 'a suitcase busting open and marbles running out.' captain states that the cabin attendant's account and the absence of any further cockpit warning indications confirmed that the bottle had discharged. (The bottle will first discharge, then the system provides a 30 min trickle charge.) ATC was advised of the aircraft's problem. A follow-up letter to the reporter, from the fleet manager, stated that the detector had been replaced.
Original NASA ASRS Text
Title: AN SF34 FLC RECEIVED A CARGO SMOKE WARNING DURING CLB. FLT WAS DIVERTED FOR ACFT EQUIP PROB CARGO COMPARTMENT SMOKE DETECTION.
Narrative: CLBING OUT OF 13000 FT, APPROX 40 NM NNW OF FSM, THE CARGO SMOKE WARNING ILLUMINATED ON CENTRAL WARNING PANEL. BOTTLE #1 FOR CARGO COMPARTMENT WAS ACTIVATED AND ASSOCIATED CHKLIST PERFORMED. AFTER APPROX 30 SECONDS, THE CENTRAL WARNING PANEL LIGHT WENT OUT. FSM HAD BETTER WX AND A LONGER RWY, AND THIS WOULD BE A STRAIGHT LINE DSCNT FOR US INSTEAD OF FYV, RIGHT BELOW US (A SPIRAL DSCNT). 12 MINS LATER WE LANDED WITHOUT INCIDENT IN FMS. #2 BOTTLE WAS NOT USED. NO EMER DECLARED. MAINT INSPECTED ACFT AND WE FERRIED IT TO DFW LATER. GREAT CREW COORD. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: A MALFUNCTIONING DETECTOR IN THE CARGO COMPARTMENT CAUSED A FALSE ALARM. THE PHOTOELECTRIC CELL IN THE SF340 CARGO COMPARTMENT WILL DETECT SMOKE, AEROSOL, THICK FUMES, AND EVEN HIGH HUMIDITY. RPTR STATES THAT 'WHEN THE PARTICLE INTERRUPTION DISSIPATES, THEN THE ALARMS WILL GO OUT.' THE WARNING IS, ITSELF, ASSOCIATED WITH A MEMORY CHKLIST ITEM FOR WHICH THE FLC FOLLOWED ALL PROCS. SHORTLY AFTER THE FLC HAD FIRED THE BOTTLE AND HAD BEGUN THE 30 SECOND TIMING, THE FLT ATTENDANT CALLED AND STATED THAT HE HEARD A WEIRD NOISE IN THE CARGO COMPARTMENT. IN FACT HE DESCRIBED THE SOUND AS 'A SUITCASE BUSTING OPEN AND MARBLES RUNNING OUT.' CAPT STATES THAT THE CABIN ATTENDANT'S ACCOUNT AND THE ABSENCE OF ANY FURTHER COCKPIT WARNING INDICATIONS CONFIRMED THAT THE BOTTLE HAD DISCHARGED. (THE BOTTLE WILL FIRST DISCHARGE, THEN THE SYS PROVIDES A 30 MIN TRICKLE CHARGE.) ATC WAS ADVISED OF THE ACFT'S PROB. A FOLLOW-UP LETTER TO THE RPTR, FROM THE FLEET MGR, STATED THAT THE DETECTOR HAD BEEN REPLACED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.