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|
Attributes | |
ACN | 318914 |
Time | |
Date | 199510 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : sea |
State Reference | WA |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | B727 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : preflight |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | other personnel other |
Qualification | other other : other |
ASRS Report | 318914 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | non adherence : published procedure non adherence : far |
Independent Detector | other other : unspecified |
Resolutory Action | none taken : detected after the fact |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Crew reported on aircraft nxx (B727) that the constant speed drive oil cooler switch would not lock in ground off position. They said they had to manually hold it in ground off for takeoff. Sea maintenance called me to defer #2 constant speed drive ejector valve inoperative. I thought this would take care of the problem so I let them defer it per MEL. I thought switch was ok when #2 was inoperative. After takeoff, realized problem was the switch and all 3 valves are affected. Flight crew was informed in-flight and first landing station (ord) item was corrected (replaced switch). Ord was next scheduled stop. I should have questioned sea maintenance further to be sure we both fully had the problem fully analyzed and correct.
Original NASA ASRS Text
Title: THE RPTR, A MECH, VIA TELEPHONE ERRED IN ALLOWING BOEING 727 TO DEPART UNDER MEL.
Narrative: CREW RPTED ON ACFT NXX (B727) THAT THE CONSTANT SPD DRIVE OIL COOLER SWITCH WOULD NOT LOCK IN GND OFF POS. THEY SAID THEY HAD TO MANUALLY HOLD IT IN GND OFF FOR TKOF. SEA MAINT CALLED ME TO DEFER #2 CONSTANT SPD DRIVE EJECTOR VALVE INOP. I THOUGHT THIS WOULD TAKE CARE OF THE PROB SO I LET THEM DEFER IT PER MEL. I THOUGHT SWITCH WAS OK WHEN #2 WAS INOP. AFTER TKOF, REALIZED PROB WAS THE SWITCH AND ALL 3 VALVES ARE AFFECTED. FLC WAS INFORMED INFLT AND FIRST LNDG STATION (ORD) ITEM WAS CORRECTED (REPLACED SWITCH). ORD WAS NEXT SCHEDULED STOP. I SHOULD HAVE QUESTIONED SEA MAINT FURTHER TO BE SURE WE BOTH FULLY HAD THE PROB FULLY ANALYZED AND CORRECT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.