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|
Attributes | |
ACN | 323416 |
Time | |
Date | 199512 |
Day | Sun |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : gcm |
State Reference | FO |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | B727 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 323416 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | other anomaly other |
Independent Detector | other controllera other flight crewa |
Resolutory Action | aircraft : equipment problem dissipated |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
On touchdown in gcm I placed all 3 engines in reverse. I inadvertently went through the gate to about 90 percent N1 momentarily where I believe I induced a compressor stall in one of the engines. Tower reported seeing flames coming out of an engine right after touchdown then go out. Rollout, taxi and shutdown were all normal. Flight attendants reported a few banging noises on touchdown. At this point I was of the firm opinion I had induced a compressor stall by improper operation. It was my decision that the engines were ok. I decided to consult with maintenance the next morning. I briefed maintenance on the incident and we decided everything was fine and to make an information to maintenance, which I did and briefed the mechanic meeting the flight. I now feel I should have had contract maintenance have a look at the aircraft that night for a more conservative exercise in safety instead of relying on my experience. At the very least I am sure seeing flames come from an engine in the dark of night was a spectacle which should have been dealt with in a more regimental manner. I do in turn believe I was running a safe operation and I do take full responsibility.
Original NASA ASRS Text
Title: PLT INADVERTENTLY APPLIED TOO MUCH REVERSE WHICH CAUSED A COMPRESSOR STALL.
Narrative: ON TOUCHDOWN IN GCM I PLACED ALL 3 ENGS IN REVERSE. I INADVERTENTLY WENT THROUGH THE GATE TO ABOUT 90 PERCENT N1 MOMENTARILY WHERE I BELIEVE I INDUCED A COMPRESSOR STALL IN ONE OF THE ENGS. TWR RPTED SEEING FLAMES COMING OUT OF AN ENG RIGHT AFTER TOUCHDOWN THEN GO OUT. ROLLOUT, TAXI AND SHUTDOWN WERE ALL NORMAL. FLT ATTENDANTS REPORTED A FEW BANGING NOISES ON TOUCHDOWN. AT THIS POINT I WAS OF THE FIRM OPINION I HAD INDUCED A COMPRESSOR STALL BY IMPROPER OP. IT WAS MY DECISION THAT THE ENGS WERE OK. I DECIDED TO CONSULT WITH MAINT THE NEXT MORNING. I BRIEFED MAINT ON THE INCIDENT AND WE DECIDED EVERYTHING WAS FINE AND TO MAKE AN INFO TO MAINT, WHICH I DID AND BRIEFED THE MECH MEETING THE FLT. I NOW FEEL I SHOULD HAVE HAD CONTRACT MAINT HAVE A LOOK AT THE ACFT THAT NIGHT FOR A MORE CONSERVATIVE EXERCISE IN SAFETY INSTEAD OF RELYING ON MY EXPERIENCE. AT THE VERY LEAST I AM SURE SEEING FLAMES COME FROM AN ENG IN THE DARK OF NIGHT WAS A SPECTACLE WHICH SHOULD HAVE BEEN DEALT WITH IN A MORE REGIMENTAL MANNER. I DO IN TURN BELIEVE I WAS RUNNING A SAFE OP AND I DO TAKE FULL RESPONSIBILITY.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.